Near Miss Reports

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 Injury Date Injury Time State Township/City Pad Latitude Longitude 911 Address Weather Well Lease Well Number Well Field Personnel/Witness Name Company Position Days Into Hitch Years With Company Years In Oil/Gas Personnel/Wittness Phone Task Summary Witness Name Witness Statement Contributing Factors Notification Timeline Corrective Action Photos & Videos Supervisor Name Supervisor Email Supervisor Phone Supervisor Office Phone HSE Name HSE Email HSE Phone HSE Office Phone Comp. Man Name Comp. Man Email Comp. Man Phone Comp. Man Office Phone NNE Name NNE Email NNE Phone NNE Office Phone NNE HSE Name NNE HSE Email NNE HSE Number NNE HSE Office Phone SUBMITTEE
07/13/202102:45 PMWVBattelleERP Pipe line @ Pad39.67355296-80.273581231 Happy Lane Fairview, WV 26570clearERP Well Pad Water LineERP water lineBattelleRodney VarnerForquer ContractingForeman1022(304) 288-2337

Hauling logs to landing area with log skidder. Skidder upset.

Russell Beach (304) 692-9552 was operating a log skidder with a load of logs. The skidder upset on its side as a result of the heavy load and un even terrain.

Rodney Varner

"Dragging logs into landing he turned down road bank. The logs were still up on road and he lifted back of skidder up. Skidder fell onto its side"

Heavy load. Un level ground30 minutesDo not turn sharp with loads. Smaller loads.Mike ReedEmail hidden; Javascript is required.(304) 288-2337(304) 879-5251Jordy ForquerEmail hidden; Javascript is required.(304) 216-5172(304) 879-5251Mike ShreveEmail hidden; Javascript is required.(304) 918-3050(304) 212-0432David McDougalEmail hidden; Javascript is required.(304) 941-5033(304) 212-0419Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415Dave McDougal
07/01/202111:05 AMWVBlacksvilleLemley39.657114480.1696953781 Long Drain Rd, Fairview, WV 26570Partly SunnyLemley1HBlacksvilleRob CowgerNNEConsultant10225(304) 276-2139

Fracing Stage 42 on the Lemley 1H

During 2.0 lb 100 Mesh on stage 42 on the 1H the turbine caught fire internally. A loud noise was heard from inside the data van, and smoke was seen coming from the turbine. All equipment was immediately shut down. Power Generation also called to shutdown. At this point flames were seen coming from the exhaust of the turbine. Gas supply was shut in, and the 1H and 3H wells were shut in. All nonessential personnel were sent to the muster area, and the onsite NNE consultant called 911 and NNE management. The fire was contained inside the turbine structure, and some small spot fires were visible on the containment from leaking oil. The fire suppression system inside the turbine actuated and smothered the fire internally. The small spot fires were controlled with fire extinguishers. Once the fire department arrived, the fire had already been suppressed. Once the turbine structure cooled to 100 deg F, the fire department opened the turbine doors to confirm the fire was completely out.

Rob Cowger

During 2.0 lb 100 Mesh on stage 42 on the 1H the turbine caught fire internally. A loud noise was heard from inside the data van, and smoke was seen coming from the turbine. All equipment was immediately shut down. Power Generation also called to shutdown. At this point flames were seen coming from the exhaust of the turbine. Gas supply was shut in, and the 1H and 3H wells were shut in. All nonessential personnel were sent to the muster area, and the onsite NNE consultant called 911 and NNE management. The fire was contained inside the turbine structure, and some small spot fires were visible on the containment from leaking oil. The fire suppression system inside the turbine actuated and smothered the fire internally. The small spot fires were controlled with fire extinguishers. Once the fire department arrived, the fire had already been suppressed. Once the turbine structure cooled to 100 deg F, the fire department opened the turbine doors to confirm the fire was completely out.

Investigation PendingImmediateInvestigation PendingCriss VanGilderEmail hidden; Javascript is required.(405) 757-8725(405) 757-8725Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 951-0909Rob CowgerEmail hidden; Javascript is required.(304) 276-2139(304) 276-2139Criss VanGilderEmail hidden; Javascript is required.(405) 757-8725(405) 757-8725Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415Criss VanGilder
08/07/202106:00 AMWVBlacksvilleERP39.634801-80.28665331 Happy Ln Fairview, WVClear, warmERP4HBlacksvilleJosh AngelineNNEConsultant5115(501) 581-1811

Loading bha onto catwalk

While loading bha onto catwalk, rig hand backed front end loader into the flange of the flow line causing damage to the rear of the loader

Josh Angeline

While loading bha onto catwalk, rig hand backed front end loader into the flange of the flow line causing damage to the rear of the loader

No spotter was utilized.Damaged was not reported. Discovered on the next shift.Utilize a spotter in tight areas of operationBobby GilbertEmail hidden; Javascript is required.(903) 486-2689(903) 486-2689Mario ElizondoEmail hidden; Javascript is required.(878) 218-8696(878) 218-8696Josh AngelineEmail hidden; Javascript is required.(501) 581-1811(501) 581-1811Josh DaltonEmail hidden; Javascript is required.(724) 825-6859(724) 825-6859Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415Josh Dalton
11/07/201909:20 AMWVBlacksvilleBoggessnananachilly about 45 degreesBoggessPadBlacksvilleTruck DriverMountaineer WeldingTruck Driver100512(000) 000-0000

Truck Driver

Tractor and Trailer hauling telehandler off site did not adhere to “no left turns” sign and turned left onto Rt 7. A rock truck came around the turn on Rt. 7 from the left having to brake excessively to keep from causing an accident. No injuries or damages reported.

Mike Pitzer (DTE)

Around 9:20am, a lowboy with large equipment was turning left out of the Boggess well pad entrance. As the lowboy was turning out, a stone truck was traveling north on Rt 7 and when they came around the corner they had to slam on their brakes and came close to impacting the lowboy. Mike was 2 trucks behind the stone truck and had to slam on his brakes as well to avoid an accident. Mike relayed that there were no impacts or injuries at all.

Did not adhere to no left turn sign2 hrsMountaineer Welding was taking actions internallyAdam BurkhammerEmail hidden; Javascript is required.(304) 266-2479(304) 452-9760na naEmail hidden; Javascript is required.(000) 000-0000(000) 000-0000John LandisEmail hidden; Javascript is required.(304) 212-0434(304) 216-6854John LandisEmail hidden; Javascript is required.(304) 212-0434(304) 216-6854Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415John Landis
10/27/201909:30 AMWVBlacksvilleCumminsN 423926.23E 1776776.64Yank Hollow Road Fairview, WV 26570Cool/showersCummins8HBlacksvilleTravis CasnerComplete EnergyDriver424(304) 514-3726

Loading up Stallion living quarters.

While winching on a stallion living quarters, the dogs on the trucks winch released and allowed the trailer to drop to the ground, trailer fell approximately 1 foot. Inside of living quarters the ceiling tiles fell down and the toilet was shattered and the sink broke.

Travis Casner

While winching up the trailer, the dogs in the main winch released allowing the winch to free spool and the trailer to fall to the ground.

mechanical failureimmediatleyLoad assisted remaining camps with the craneTom PoseyEmail hidden; Javascript is required.(304) 514-3726(304) 514-3726Brent PhillipsEmail hidden; Javascript is required.(740) 502-1218(740) 502-1218Joshua GrimEmail hidden; Javascript is required.(304) 276-3899(304) 276-3899Joshua DaltonEmail hidden; Javascript is required.(724) 825-6859(724) 825-6859Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415
10/23/201903:10 AMWVBlacksvilleBoggess39.67012280.093442030 Mason Dixon Hwy, Maidsville, WV 26541Cloudy 48 degreesBoggess9HBlacksvilleGlen Boyd BoydNNEConsultant14430(304) 481-2344

Drill Out Ops - Completed sweep at PBTD, Beginning trip out

Night shift had drilled all 59 plugs. Pulled and layed down Jt 635. Made up Jt 634 on the swivel to begin the surface to surface sweep while working the PH6 work string. At this point the saver sub and joint 634 seperated. The mud pump was SD and the pipe ram on the BOP's was shut. The WS fell and lodged into the annular bag which in return damaged the bag. Once everone was asked if they were OK the snubbers screwed a pup jt into the WS and pulled it back into the heavy slips and made up the kelly line to a Pump In Sub/TIW valve on joint 634 and continued the surface to surface sweep. Once the STS was completed we pulled Jt 634 and put it out of service.

Jeremy Fakourey

Working 2nd from last joint up from bottom when the saver sub at the swivel blew apart from the work string joint on upstroke

Possibly burnt/gaulded the threads when they MU the Jt.4 HrsDeemed the saver sub and Jt 634 out of service. Contacted KLX to come out to location to inspect and guage the threads on the WS.Criss VanGilderEmail hidden; Javascript is required.(405) 757-8725(405) 757-8725Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 951-0909Glenn BoydEmail hidden; Javascript is required.(304) 481-2344(304) 481-2344Criss VanGilderEmail hidden; Javascript is required.(405) 757-8725(405) 757-8725Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415Criss VanGilder
08/22/201907:00 AMWVBlacksvilleKassaynanaBlacksville WVwarmKassay5HBlacksvilleSteve CollinsNNEWell Tender365310(304) 413-5721

Well Tender

Kassay 5H had a valve that cut out and was releasing gas. The men from the rig staying there heard and smelled gas and ESD'd Pad. As they ESD's the pad.......there was also an alarm for low separator pressure from the vessel which would have ESD'd the well. Steve went to location, Identified the problem and fixed the valve.

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Investigating/Sand over time.within 2 hrsYes. fixed valveJohn LandisEmail hidden; Javascript is required.(304) 216-6854(304) 212-0434Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415na naEmail hidden; Javascript is required.(000) 000-0000(000) 000-0000na naEmail hidden; Javascript is required.(000) 000-0000(000) 000-0000Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415John Landis
07/08/201905:30 PMWVBlacksvilleKassayN39°39'09.20"W80°12'35.22"25 Yank Hollow Rd. Fairview, WVClearKassayN/ABlacksvilleDonnie ShamblinComplete Energy ServicesDriver51.53(304) 203-8895

unload roller truck holding two upright clean harbors tanks.

While pulling the two Clean harbors tanks off of the roller truck to stage at the Kassay Pad, the operators(Chris Wayne, Jake Fields, and Donnie Shamblin) chained both tanks together to pull them off of the truck. The front tank began to slide to the right and fell uncontrolled to the ground off of the truck damaging the top of the tank and the valve assembly at the bottom.

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inability to get to load hooks on the rear tank during unloadingImmediatelyHaul a single tank that way load hook is accessible.Tom PoseyEmail hidden; Javascript is required.(740) 891-8251(740) 891-8251Tom PhillipsEmail hidden; Javascript is required.(740) 891-8251(740) 891-8251Joshua GrimEmail hidden; Javascript is required.(304) 276-3899(304) 276-3899Josh DaltonEmail hidden; Javascript is required.(724) 825-6859(304) 212-0424Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415Josh Dalton
07/02/201902:45 PMWVBlacksvilleBoggess39.667166-80.0968461709 Mason Dixon Hwy Morgantown, WV 26541Hot/thunderstorms with lightning less than 3 miles from locationBoggess17HBlacksvilleEdward SineChisler Brothers TruckingDriver2232(304) 612-6352

Loading a frac tank onto a bobtail truck to haul from the Boggess Pad to the Cummins Pad.

During a lightning shutdown, Edward Sine arrived on location without checking in with the job site supervisor and began loading an empty frac tank that had a guide wire attached to the top of the tank going up to the weight bucked attached to the derrick climb assist. He than proceeded to pull forward and noticed that there was something pulling on his load. He stepped on the brake and clutch and the pad eye located on the top of the tank at the point of attachment broke releasing the cable which snapped back and wrapped itself around the boom winch at the crown of the rig as rig personnel returned to work from being sheltered from the storm. Work was immediately stopped and the situation was investigated by Rig manager(Steve Tichey) and Co. Man(Josh Grim).

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Rain/poor visibility. Failure to check in to be informed of operations.ImmediatelyDerrick hand climbed and visually inspected all points of attachment in the derrick and guide cable that was accessible.Bruce ChislerEmail hidden; Javascript is required.(304) 282-0048(304) 879-5011Bruce ChislerEmail hidden; Javascript is required.(304) 282-0048(304) 879-5011Joshua GrimEmail hidden; Javascript is required.(304) 276-3899(304) 276-3899Josh DaltonEmail hidden; Javascript is required.(724) 825-6859(304) 212-0424Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415Josh Dalton
02/05/201911:30 AMWVBlacksvilleMepco39.662862-80.152454579 Mepco Road, Fairview, WV 26570OvercastMepcoMepcoBlacksvilleJeff WilsonSolo ConstructionWater Consultant51111(304) 480-1414

Rigging down water transfer after drillout operations concluded.

Jeff Wilson had suspicion that Jessie Botti, an SES employee, was under the influence of something based on a conversation and observing his actions, so he called the employee's supervisor to determine. The supervisor had reasonable suspicion that he was under the influence and took him for a drug screen. The employee had a BAC of 0.23 (legal limit is 0.08) and was immediately terminated.

Jeff Wilson

"This morning on Mepco I arrived on location and had a boy from Select approach me and started asking me questions about his work for the day. He didn't seem quite right so I kept an eye on him . He seemed like he was having trouble holding his train of thought. When he would bend over he would lose his balance and have to catch himself.
I contacted Cassey and told him I didn't want to accuse the boy of being under the influence of anything not knowing the boy. I asked Cassey to send someone to location that knew him to just have a conversation with him and get their opinion. Another boy showed up and I explained to him not to ask if he had been doing anything or accuse him of anything but just get him in a truck and talk to him. After 5 min the boy came to me and said that he believed he was under the influence of something and that they were taking him for drug screen. He said the boy was having some difficulty speaking and when he was asked to fill out JSA he couldn't write. The boy left with him and they were meeting Cassey and cassey was taking him for drug screen."

First day back to work after having three days off prior to.10:00 AM, encounter occurred; 11:27 AM, Jeff notified Chris Patterson; 1:32 PM, SES notified NNE of drug screen result and subsequent termination.Employee terminatedCasey BuchananEmail hidden; Javascript is required.(304) 224-5567(304) 224-5567Chuck BerdineEmail hidden; Javascript is required.(724) 914-3814(724) 914-3814Jeff WilsonEmail hidden; Javascript is required.(304) 480-1414(304) 480-1414Chris PattersonEmail hidden; Javascript is required.(304) 203-7034(304) 212-0417Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415Chris Patterson
10/11/201811:51 AMWVBlacksvilleJenkinsNANABlacksville WVsunnyJenkins2,4,6,8,10,14,18BlacksvilleBrian MeadowsNNEWell Tender4115(304) 685-6995

Well Tender

Pulled up on pad and thought a dump was stuck open. Went into unit and ball valve blew out side. Shut in Unit and the unit blew down. Within a couple of hours later another ball valve blew and a 2" Balon Dump Valve. The pad was then shut in until all units have been repaired and inspected.

Josh Frazier

As I was coming up the lease road towards the pad, I noticed a big fog above the pad and heard a very loud hissing sound as well. As I got closer I could barely see a few people off to the side of Pad and went over to see what was going on once I saw that it was safe. Brian was pretty shook up and said another dump/bypass valve had blown apart on the GPU (#4) while he was standing inside of it. He was hit by some sand, water and some loud noises but is fine as of now. With help from Dave and the ShalePro guy on location, they isolated the unit. There was also a Nalco employee taking samples right before the incident. Luckily, no one was injured.

Investigating/Sandwithin 2 hrsYes. Pad was shut in and unit bled down entire pad. Work and inspection being completed on units before flowing through them again.John LandisEmail hidden; Javascript is required.(304) 216-6854(304) 212-0434Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415John LandisEmail hidden; Javascript is required.(304) 216-6854(304) 212-0434John LandisEmail hidden; Javascript is required.(304) 216-6854(304) 212-0434Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415John Landis
10/08/201809:57 AMWVBlacksvilleYostNANABlacksville WVsunnyYost3HBlacksvilleBrian MeadowsNNEWell Tender4115(304) 552-9023

Well Tender

Found a dump had blown out bottom and through top of reservoir inside GPU.

Brian Meadows

Found a dump had blown out bottom and through top of reservoir inside GPU. Gas was blowing out of unit so the ESD button was pressed to shut in pad.

Investigatingwithin 2 hrsYes. Pad was shut in and unit bled down through line to tanks. Dump and reservoir were fixed before turning back on the well.John LandisEmail hidden; Javascript is required.(304) 216-6854(304) 212-0434Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415John LandisEmail hidden; Javascript is required.(304) 216-6854(304) 212-0434John LandisEmail hidden; Javascript is required.(304) 216-6854(304) 212-0434Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415John Landis
09/18/201812:00 PMWVBlacksvilleMepco39 39 45.9380 09 07.77579 Mepco Road, Fairview, WV 26570Rain overcastMEPCOLease RdBlacksvilleMichael KnightExport FuelDriver553(724) 610-1532

Driver had just offloaded fuel on the Mepco pad and was leaving on the lease rd. The driver stated he reached down for his Pepsi and the truck dropped off the left side of the road and bottomed out in the ditch line. Hillbilly towing was called and was able to remove the fueler from the ditch.

Driver had just offloaded fuel on the Mepco pad and was leaving on the lease rd. The driver stated he reached down for his Pepsi and the truck dropped off the left side of the road and bottomed out in the ditch line. Hillbilly towing was called and was able to remove the fueler from the ditch. No injuries, environmental releases, vehicle, or property damage.

Shane Stephenson

Driver had just offloaded fuel on the Mepco pad and was leaving on the lease rd. The driver stated he reached down for his Pepsi and the truck dropped off the left side of the road and bottomed out in the ditch line. Hillbilly towing was called and was able to remove the fueler from the ditch.

Not paying attentionImmediatelyDriver will not return to location. Safety meeting was held discussing driver safetyShane StephensonEmail hidden; Javascript is required.(405) 757-8725(405) 757-8725Shane StephensonEmail hidden; Javascript is required.(405) 757-8725(405) 757-8725Eric BooneEmail hidden; Javascript is required.(304) 377-6666(304) 377-6666Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415Criss VanGilder
09/01/201812:05 AMWVBlacksvilleYost39.6296-80.2149218/Daybrook Run Rd.75 deg / NightYost7HBlacksvilleCharles FugateHighlandsTool Pusher5815(304) 890-5197

Moving center tub out away from the rig.

Charles (Night Tool Pusher) was operating the John Deere front loader to move the center tub away from the rig to pull the HCR off the mud cross. Placed forks underneath the center tub on ODS of the rig. While backing up the front steer tires transitioned from the matting boards to the cellar plates. Deflecting the cellar plates the forks tilted down and slid the center tub off. Tub slid down and pushed the corner of the rig mats into the 5H cage. The impact moved the cellar cage 2' contacting the 2" casing pressure line. Pulled the threads off the 2"nipple between the valve and elbow releasing ~600 psi of pressure. Charles immediately moved the fiberglass cellar cover and closed the valve.

Charles Fugate

While moving the center tub my forks tilted forward after driving onto the cellar plate. Causing the tub to slide off the forks and push the matting boards into the cellar cage. I heard a hissing noise and immediately moved the grating and closed the 2" valve in the cellar.

Driving over cellar with (2) 1/2" cellar plates with a full load.Tool Pusher notified Ross Drnjevich immediatly after the incedent.Do not drive over cellars with any equipment. Place equipment between cellars on solid ground. Center tub will be moved one end at a time.alvin WilsonEmail hidden; Javascript is required.(304) 539-1883(000) 000-0000Mike LawrenceEmail hidden; Javascript is required.(304) 542-8238(000) 000-0000Ross DrnjevichEmail hidden; Javascript is required.(724) 579-9683(000) 000-0000Jay HewittEmail hidden; Javascript is required.(304) 382-1825(000) 000-0000Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415
08/28/201809:15 AMWVBlacksvilleYost39.641739-80.2182173589 Daybrook Rd. Fairview, WV 26570Clear and Sunny, HotYost7HBlacksvillewill AbrahamBills BitsDriver(412) 518-8405

Delivering soap tote to location

As the Bill's Bit service driver(William Abraham - (412)518-8405) was pulling onto a congested location, he thought he could squeeze through a tighter spot with his truck and trailer and grazed the bumper of a parked pickup truck belonging to a floorhand(Grover Clawson - (740)434-32432).

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Congested location, impatience/in a hurryNotified immedietley after everyone was confirmed safe/ok.Drivers swapped out insurance information and phone numbers.00000000000 0000000000Email hidden; Javascript is required.(000) 000-0000(000) 000-00000000000000 000000000000Email hidden; Javascript is required.(000) 000-0000(000) 000-0000Josh GrimEmail hidden; Javascript is required.(304) 276-3899(000) 000-0000Jay HewittEmail hidden; Javascript is required.(304) 382-1825(000) 000-0000Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415
04/11/201805:15 PMWVBlacksvilleJenkins39.7162-80138073726 Mason Dixon Hwy Morgantown, WV 26541Clear and breezy, 50°JenkinsmoveBlacksvilleandy travis(000) 000-0000

After loading the Strad upright tanks to be taken back to the Strad yard

After loading the Strad upright tanks to be taken back to the Strad yard, one of the trucks struck a low phone line along route 7. The pilot car noticed the low line and tried to notify the driver(Jamie Jones 304-488-6978) but the driver never heard the notification and continued through snagging the line and breaking it. Immedietley afterwards Timothy James notified his HSE, the Utility company, and myself.

00000 00000low lines/ faulty communicationNotified immediate after it everything was confirmed safeverify equipment is working properly or get a confirmation that the order was heard by driverTimothy "Cowboy" JamesEmail hidden; Javascript is required.(000) 000-0000(000) 000-0000Brent PhillipsEmail hidden; Javascript is required.(740) 502-1218(000) 000-0000Joshua GrimEmail hidden; Javascript is required.(304) 276-3899(000) 000-0000Jay HewittEmail hidden; Javascript is required.(304) 382-1825(000) 000-0000Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415
03/22/201709:16 PMWVBlacksvilleI79 south 121 mile postBlacksville

While driving south on I79 in traffic. A piece of debri struck the windshield of my 2014 f150 on the passenger side causing a chip in the windshield I looked at the vehicles around me and did not notice any vehicles with excessive mud on them

Andy Travis
04/09/201708:00 PMWVBlacksvilleBlacksville

At approximately 1600 PM on 4/9/17, Best Line Equipment rentals was delivering a tele-handler to the Kassay Pad. The driver, Justin, had lowered his drop trailer and unloaded the tele-handler. Justin then attempted to raise his drop trailer. He then noticed the trailer was not working and had released approximately 15-20 gallons of hydraulic fluid onto the Kassay pad. The roustabout also noticed it at the same time and put a duck pond under the trailer. The roustabout continued to contain the hydraulic fluid and the driver reported it to me. We immediately contained with peat moss and began to dig up the fluid and put it a waste dumpster. We have contacted Max with NGE to evaluate the material and the cleanup. I have attached before pictures and we will follow up with after pictures when we can.

Non- Hazardous Release (Hydraulic oil approximately 15-20 gallons)
73 Degs, Clear and sunny no wind
Was placed in a Waste Container.
Pad was dry at the time of release.

Andy Travis
04/30/201701:36 AMWVBlacksvilleBlacksville

At 21:36 hrs we had an incident while running 5.5 production casing. After latching up a joint of casing on the cat walk with the elevators the Driller began to pick up the joint during that time he floated his elevators back in as normal. At the same time the derrick hand that was operating the cat walk and skate, ran the skate up to far and pushed the joint of casing thru the elevators into the back of the derrick. The driller could not see that the casing had went into the back of the derrick underneath one of the 4X4 beams in the top drive track. The casing struck the beam while coming up and ripped it free from the I beams of the top drive track, the 4X4 beam fell to the floor landing on the rotary table. Kimzy casing crew had 3 men that were working on the floor where the beam fell to the floor, they saw it happen and were able to dive out of the way of the beam before it came to the floor.

Myself and the Rig Manager heard the incident happen and immediately went to the rig floor to assess the situation and ensure no one was injured (no injuries). It was found that the top drive track had suffered damage and was bent to the point that the top drive could not come to the floor. (Jay Hewitt was contacted at this time)( Brent Kasmiear Nabors superintendent)

We held a safety stand down to allow the personal to calm down and come up with a plan to remove the joint of casing that was still latched in the elevators. Once a plan was in place we removed the joint of casing and rigged down the casing crew and began circulating the casing.

Andy Travis
05/07/201711:45 AMWVBlacksvilleBlacksville

While pressure testing for stage 20 on the Kassay 7H a wing ? on the back of one of the pumps failed catastrophically. Test pressure was 10,657 psig at the time of failure. No one was in the red zone during the incident.

Andy Travis
06/19/201704:58 PMWVBlacksvilleBlacksville

BJ Services employee was performing preventative maintenance on a fluid end. While making the repairs another employee asked him a question, he turned his head to answer the question and the plunger fell and struck him the foot. The injured employee was wearing steel toe/metatarsal boots, but still sustained an injury. The employee was taken to the supervisors truck, Axiom and BJ EHS were notified, first aid and icing the foot were recommended. The employee later decided to have an x-ray 6/22/2017, which revealed a hair line fracture.

Andy Travis
07/03/201708:53 PMWVBlacksvilleYank Hollow Road Dave Dillie's trailerBlacksville

I received a complaint from Dave Dillie on July 3,2017. He alleges NNE has caused the floor in his trailer to start to wave, He said he checked the frame, where he could access it with the level, but agreed the frame was level. The allegations started that by drilling under it we changed the water table, which then caused the trailer to settle. After further discussion and the talking through the process of drilling, he claimed it was the sand truck traffic beating on the ground that caused the trailer to settle. I told him I would discuss it with the office and we would get back to him. 7-6-2017 I went out to look at the fence that we needed to reinstall and his daughter asked what we had decided on the trailer. I told her the issue was still being discussed and we would get back to them. Mrs, Dillies cell phone #304-692-5613

Andy Travis
08/14/201707:30 AMWVBlacksvilleKassay Pad/DTE InterconnectBlacksville

DTE's pipeline has a pressure release valve at the interconnect below the Kassay Pad. The valve is set to "pop off" at 1200 psig. Our Kassay pad has a pressure safety high on our pad set at 1150 psig. So, our pad should shut in before the pressure release valve goes off shutting in our pad. The pressure safety high had been disabled and the pressure on the pipleline got above 1200 psig, causing the pressure relief valve to actuate. This venting of gas startled the water truck drivers and they ESD's the pad, which was the correct form of action. Going forward the pressure safety high on the pipeline pressure for the Kassay pad will not be disabled.

Andy Travis
09/05/201702:40 PMWVBlacksvilleBlacksville

A tandem from Lightening trucking was unloading the compressor off the bed, the bridal didn't have enough slack in it so it came off the ear of the skid. When it did the radiator of the compressor was bent. No one was in the red zone and no other equipment was damaged.

Andy Travis
10/03/201703:45 PMWVBlacksvilleBlacksville

I just received word from the field that one of the water truck drivers from Ransom Drilling was killed as a result of his truck wrecking. I?m told as he was traveling on Rt. 50 to/from one the disposal facilities in Ohio, the truck blew a tire and he lost control. DOT is on scene and will conduct an investigation. There is a story already on WBOY?s website with two pictures, as well as WDTV?s website.

Andy Travis
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