Near Miss Reports

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 Injury Date Injury Time State Township/City Pad Latitude Longitude 911 Address Weather Well Lease Well Number Well Field Personnel/Witness Name Company Position Days Into Hitch Years With Company Years In Oil/Gas Personnel/Wittness Phone Task Summary Witness Name Witness Statement Contributing Factors Notification Timeline Corrective Action Photos & Videos Supervisor Name Supervisor Email Supervisor Phone Supervisor Office Phone HSE Name HSE Email HSE Phone HSE Office Phone Comp. Man Name Comp. Man Email Comp. Man Phone Comp. Man Office Phone NNE Name NNE Email NNE Phone NNE Office Phone NNE HSE Name NNE HSE Email NNE HSE Number NNE HSE Office Phone SUBMITTEE
03/22/201709:16 PMWVBlacksvilleI79 south 121 mile postBlacksville

While driving south on I79 in traffic. A piece of debri struck the windshield of my 2014 f150 on the passenger side causing a chip in the windshield I looked at the vehicles around me and did not notice any vehicles with excessive mud on them

Andy Travis
04/09/201708:00 PMWVBlacksvilleBlacksville

At approximately 1600 PM on 4/9/17, Best Line Equipment rentals was delivering a tele-handler to the Kassay Pad. The driver, Justin, had lowered his drop trailer and unloaded the tele-handler. Justin then attempted to raise his drop trailer. He then noticed the trailer was not working and had released approximately 15-20 gallons of hydraulic fluid onto the Kassay pad. The roustabout also noticed it at the same time and put a duck pond under the trailer. The roustabout continued to contain the hydraulic fluid and the driver reported it to me. We immediately contained with peat moss and began to dig up the fluid and put it a waste dumpster. We have contacted Max with NGE to evaluate the material and the cleanup. I have attached before pictures and we will follow up with after pictures when we can.

Non- Hazardous Release (Hydraulic oil approximately 15-20 gallons)
73 Degs, Clear and sunny no wind
Was placed in a Waste Container.
Pad was dry at the time of release.

Andy Travis
04/30/201701:36 AMWVBlacksvilleBlacksville

At 21:36 hrs we had an incident while running 5.5 production casing. After latching up a joint of casing on the cat walk with the elevators the Driller began to pick up the joint during that time he floated his elevators back in as normal. At the same time the derrick hand that was operating the cat walk and skate, ran the skate up to far and pushed the joint of casing thru the elevators into the back of the derrick. The driller could not see that the casing had went into the back of the derrick underneath one of the 4X4 beams in the top drive track. The casing struck the beam while coming up and ripped it free from the I beams of the top drive track, the 4X4 beam fell to the floor landing on the rotary table. Kimzy casing crew had 3 men that were working on the floor where the beam fell to the floor, they saw it happen and were able to dive out of the way of the beam before it came to the floor.

Myself and the Rig Manager heard the incident happen and immediately went to the rig floor to assess the situation and ensure no one was injured (no injuries). It was found that the top drive track had suffered damage and was bent to the point that the top drive could not come to the floor. (Jay Hewitt was contacted at this time)( Brent Kasmiear Nabors superintendent)

We held a safety stand down to allow the personal to calm down and come up with a plan to remove the joint of casing that was still latched in the elevators. Once a plan was in place we removed the joint of casing and rigged down the casing crew and began circulating the casing.

Andy Travis
05/07/201711:45 AMWVBlacksvilleBlacksville

While pressure testing for stage 20 on the Kassay 7H a wing ? on the back of one of the pumps failed catastrophically. Test pressure was 10,657 psig at the time of failure. No one was in the red zone during the incident.

Andy Travis
06/19/201704:58 PMWVBlacksvilleBlacksville

BJ Services employee was performing preventative maintenance on a fluid end. While making the repairs another employee asked him a question, he turned his head to answer the question and the plunger fell and struck him the foot. The injured employee was wearing steel toe/metatarsal boots, but still sustained an injury. The employee was taken to the supervisors truck, Axiom and BJ EHS were notified, first aid and icing the foot were recommended. The employee later decided to have an x-ray 6/22/2017, which revealed a hair line fracture.

Andy Travis
07/03/201708:53 PMWVBlacksvilleYank Hollow Road Dave Dillie's trailerBlacksville

I received a complaint from Dave Dillie on July 3,2017. He alleges NNE has caused the floor in his trailer to start to wave, He said he checked the frame, where he could access it with the level, but agreed the frame was level. The allegations started that by drilling under it we changed the water table, which then caused the trailer to settle. After further discussion and the talking through the process of drilling, he claimed it was the sand truck traffic beating on the ground that caused the trailer to settle. I told him I would discuss it with the office and we would get back to him. 7-6-2017 I went out to look at the fence that we needed to reinstall and his daughter asked what we had decided on the trailer. I told her the issue was still being discussed and we would get back to them. Mrs, Dillies cell phone #304-692-5613

Andy Travis
08/14/201707:30 AMWVBlacksvilleKassay Pad/DTE InterconnectBlacksville

DTE's pipeline has a pressure release valve at the interconnect below the Kassay Pad. The valve is set to "pop off" at 1200 psig. Our Kassay pad has a pressure safety high on our pad set at 1150 psig. So, our pad should shut in before the pressure release valve goes off shutting in our pad. The pressure safety high had been disabled and the pressure on the pipleline got above 1200 psig, causing the pressure relief valve to actuate. This venting of gas startled the water truck drivers and they ESD's the pad, which was the correct form of action. Going forward the pressure safety high on the pipeline pressure for the Kassay pad will not be disabled.

Andy Travis
09/05/201702:40 PMWVBlacksvilleBlacksville

A tandem from Lightening trucking was unloading the compressor off the bed, the bridal didn't have enough slack in it so it came off the ear of the skid. When it did the radiator of the compressor was bent. No one was in the red zone and no other equipment was damaged.

Andy Travis
10/03/201703:45 PMWVBlacksvilleBlacksville

I just received word from the field that one of the water truck drivers from Ransom Drilling was killed as a result of his truck wrecking. I?m told as he was traveling on Rt. 50 to/from one the disposal facilities in Ohio, the truck blew a tire and he lost control. DOT is on scene and will conduct an investigation. There is a story already on WBOY?s website with two pictures, as well as WDTV?s website.

Andy Travis
10/03/201710:45 PMWVBlacksvilleBlacksville

At 6:45 pm an Aveda truck driver was unloading his last load of the day unassisted and without authorization. As the pump for the rig was being hoisted up the roller board the line broke dropping the pump approximately 7'. No one was in the area but the pump sustained damage. It bent the skid, which throws the pump out of alignment, damaged the electrical motor and damaged the gear end. It will be about four days before a replacement can be put together.

The employee has been terminated for not listening to instructions and going against policies of all three companies involved. After the incident a safety stand down was preformed.

Andy Travis
10/09/201705:00 PMWVBlacksvilleBlacksville

A Day Brook truck hauling fresh water was attempting to pas a parked pickup when it slid off the road. The driver contacted Brad Chadwick and they anchored the truck with a tandem until another water truck could empty it out. Once empty they were able to drive the truck back on the road.

The pickup was not supposed to be parked in that location and the Day Brook driver should have not made the attempt with such little clearance.

Moving forward we will make sure no one parks along the lease road.

Andy Travis
10/20/201711:15 AMWVBlacksvilleBlacksville

Today at approximately 1115AM a panhandle Casing truck was delivering 9 5/8? casing to the Coastal pad and on his way back through the fisher location, the rear of his trailer hooked the front fender of the Rig Managers truck pushing it into the safety shack. There are no injuries. The Panhandle truck was being driven by Gail See He has been driving tractor trailers since 2002. He is driving out of the Morgantown, WV dispatch phone

The red Chevrolet pickup is a Patterson company vehicle driven by Patterson #334 rig manager Jeff Donahue

Andy Travis
11/13/201710:30 AMWVBlacksvilleBlacksville

Kenneth Keeling, a Patterson UTI Motorhand was found passed out under the influence of alcohol in the passenger side front seat of a vehicle on location. Patterson UTI HSE was informed by rig manager Jeff Donahue) and a field sobriety check was performed. Kenneth blew over the legal limit. Patterson was let go and was taken to the airport by Patterson HSE.

Andy Travis
11/13/201702:00 PMWVBlacksvilleBlacksville

Travis was dumping onto the stockpile with A John Deere 250 Artic rock truck. he was slightly downhill, when he dumped the load, the load did not slide out of the truck and it tilted the cab over. there were no injuries and minimal damage to truck.

Andy Travis
11/15/201709:30 AMWVBlacksvilleBlacksville

Ryan Emery from Backwoods Oil & Gas Services, Inc. had to move a light plant from the back of location to the front utiliziing a 12k telehandler. He picked up the light plant with the telehander forks near the back of location. Light plant picked ~2' off the ground. While driving behind the KSW backyard he bumped into Jordan Neville's white F150 with his forks that was parked along the AST containment, damaging the grille and hood. All red zones were in place while equipment was in operation and seat belts were utilized.

Andy Travis
01/14/201810:45 PMWVBlacksvillePost Frac Move from Campbell Pad to Nine Energy LocationBlacksville

On January 14th at 10:45 PM while moving the Nine Energy grease trailer from the Coastal Pad up the steep hill towards the Fisher Pad, a dash light came on in the Nine Energy pickup truck indicating "Transmission Too Hot" and the engine shut off. The truck began coasting backwards downhill with no steering or brakes. The trailer turned and pulled the pickup into the ditch, then came free from the fifth-wheel ball, which parted the safety chains and the break-away latch. The pickup came to a stop in the ditch, while the trailer continued coasting downhill. The trailer remained upright as it rolled backwards and stopped right before the tree line approximately 70 yds from the lease road.

Dustin Merchant was the driver of the Nine Energy pickup. He is a hot shot driver for Nine. He was uninjured, but was taken to the hospital for examination. Dustin also underwent a drug and alcohol test last night and the results were ?negative?.

There were no releases involved with the incident. Damage to the pickup includes body damage, driveshaft and possible hidden damage. Damage to the PCE trailer appears to be minor. The trailer has been towed back to the lease road and inspected carefully. Both the truck and trailer have been removed from NNE property. Nine Energy's investigation is ongoing.

Andy Travis
11/07/201909:20 AMWVBlacksvilleBoggessnananachilly about 45 degreesBoggessPadBlacksvilleTruck DriverMountaineer WeldingTruck Driver100512(000) 000-0000

Truck Driver

Tractor and Trailer hauling telehandler off site did not adhere to “no left turns” sign and turned left onto Rt 7. A rock truck came around the turn on Rt. 7 from the left having to brake excessively to keep from causing an accident. No injuries or damages reported.

Mike Pitzer (DTE)

Around 9:20am, a lowboy with large equipment was turning left out of the Boggess well pad entrance. As the lowboy was turning out, a stone truck was traveling north on Rt 7 and when they came around the corner they had to slam on their brakes and came close to impacting the lowboy. Mike was 2 trucks behind the stone truck and had to slam on his brakes as well to avoid an accident. Mike relayed that there were no impacts or injuries at all.

Did not adhere to no left turn sign2 hrsMountaineer Welding was taking actions internallyAdam BurkhammerEmail hidden; Javascript is required.(304) 266-2479(304) 452-9760na naEmail hidden; Javascript is required.(000) 000-0000(000) 000-0000John LandisEmail hidden; Javascript is required.(304) 212-0434(304) 216-6854John LandisEmail hidden; Javascript is required.(304) 212-0434(304) 216-6854Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415John Landis
10/23/201903:10 AMWVBlacksvilleBoggess39.67012280.093442030 Mason Dixon Hwy, Maidsville, WV 26541Cloudy 48 degreesBoggess9HBlacksvilleGlen Boyd BoydNNEConsultant14430(304) 481-2344

Drill Out Ops - Completed sweep at PBTD, Beginning trip out

Night shift had drilled all 59 plugs. Pulled and layed down Jt 635. Made up Jt 634 on the swivel to begin the surface to surface sweep while working the PH6 work string. At this point the saver sub and joint 634 seperated. The mud pump was SD and the pipe ram on the BOP's was shut. The WS fell and lodged into the annular bag which in return damaged the bag. Once everone was asked if they were OK the snubbers screwed a pup jt into the WS and pulled it back into the heavy slips and made up the kelly line to a Pump In Sub/TIW valve on joint 634 and continued the surface to surface sweep. Once the STS was completed we pulled Jt 634 and put it out of service.

Jeremy Fakourey

Working 2nd from last joint up from bottom when the saver sub at the swivel blew apart from the work string joint on upstroke

Possibly burnt/gaulded the threads when they MU the Jt.4 HrsDeemed the saver sub and Jt 634 out of service. Contacted KLX to come out to location to inspect and guage the threads on the WS.Criss VanGilderEmail hidden; Javascript is required.(405) 757-8725(405) 757-8725Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 951-0909Glenn BoydEmail hidden; Javascript is required.(304) 481-2344(304) 481-2344Criss VanGilderEmail hidden; Javascript is required.(405) 757-8725(405) 757-8725Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415Criss VanGilder
07/02/201902:45 PMWVBlacksvilleBoggess39.667166-80.0968461709 Mason Dixon Hwy Morgantown, WV 26541Hot/thunderstorms with lightning less than 3 miles from locationBoggess17HBlacksvilleEdward SineChisler Brothers TruckingDriver2232(304) 612-6352

Loading a frac tank onto a bobtail truck to haul from the Boggess Pad to the Cummins Pad.

During a lightning shutdown, Edward Sine arrived on location without checking in with the job site supervisor and began loading an empty frac tank that had a guide wire attached to the top of the tank going up to the weight bucked attached to the derrick climb assist. He than proceeded to pull forward and noticed that there was something pulling on his load. He stepped on the brake and clutch and the pad eye located on the top of the tank at the point of attachment broke releasing the cable which snapped back and wrapped itself around the boom winch at the crown of the rig as rig personnel returned to work from being sheltered from the storm. Work was immediately stopped and the situation was investigated by Rig manager(Steve Tichey) and Co. Man(Josh Grim).

N/A N/A

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Rain/poor visibility. Failure to check in to be informed of operations.ImmediatelyDerrick hand climbed and visually inspected all points of attachment in the derrick and guide cable that was accessible.Bruce ChislerEmail hidden; Javascript is required.(304) 282-0048(304) 879-5011Bruce ChislerEmail hidden; Javascript is required.(304) 282-0048(304) 879-5011Joshua GrimEmail hidden; Javascript is required.(304) 276-3899(304) 276-3899Josh DaltonEmail hidden; Javascript is required.(724) 825-6859(304) 212-0424Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415Josh Dalton
04/30/201910:30 AMWVClayBoggess39.670089-80.093496000000Boggess3HBlacksvilleRobert ForceEnerstarDriver(570) 494-6277

Hauling stallion trailer to Stallion yard from Boggess Pad.

Truck driver picked up a Stallion crew accommodation that was not being used after offloading a trailer at the Mateo pad. The driver exited the pad location and drove down to route 7. The AT&T fiber line was hanging low about 14' and the driver hit the line pulling the line anchor out of the power line post. The driver then turned left onto route 7 ignoring the posted NNE signage that say's (no left turns). The Pilot car company (X5O) did not high pole the line, reason unknown.

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Human errorImediateDriver no longer permitted onsiteJared 000Email hidden; Javascript is required.(570) 567-4237(304) 951-0909Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 951-0909Troy HamidiEmail hidden; Javascript is required.(719) 459-2067(304) 951-0909Jay Hewitt IIEmail hidden; Javascript is required.(304) 382-1825(304) 951-0909Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415
05/18/202109:30 AMWVBlacksvilleBunner39.66209780.21431272 Upper Days Run Rd Fairview, WV 26570Clear, warmBunner4HBlacksvilleBobby GilbertPatterson UTIPusher1499(903) 486-2689

Removing valve seat from mud pump

On 5/18/2021 at approximately 08:45 the rig went down on MP#2 due to washed seats and valves on the #2 module. The Rig
Crew began repairs on the mud pump by removing the discharge seat successfully, and then moved onto the suction seat. At
approximately 09:30 the crew began to pressure up on the seat puller with the Pancake, as the pressure approached
9500PSI there was a sudden release at the seat puller; the all thread center stem bolt used to pull the seat separated inside
the module leaving 14” of the bolt in the module and releasing 24”s of the bolt into the air. The bolt went through the open
roof hatch and landed on top of the mud pump roof. The bolt weight was approximately 19.8 pounds.
The bolt was shipped to the manufacturer for a metallurgy inspection to help determine the root cause.
Moving forward, until a proper recommendation from the manufacturer is received, crews will establish a red zone and utilize a restraining device.

Bobby Gilbert

On 5/18/2021 at appx 08:45, the rig went down on MP #2 due to washed seats and valves on the #2 module. The rig crew began the repairs by removing the discharge seat successfully, and then moved on to the suction seat. At appx 09:30 the crew began to pressure up on the seat puller, and as the pressure approached 10,000 psi there was a sudden release at the seat puller. The all thread center stem bolt used to pull the seat had separated inside the module leaving 14'' of the bolt in the module and releasing 24''s of the bolt into the air. The mud pump room roof door was open, so the bolt went through the roof door and landing on top of the roof. The bolt weighed appx 19.8 lbs.

Excessive use of seat puller or may have had a small crack in the bolt prior to useCo. Rep Josh Angeline was notified at appx. 2:00pm. Superintendent Sam Barker was notified at 03:00pmRecommend regular inspection on seat pulling tool and have an adequate length of hose to allow rig hands to pressure up on the tool while being outside of the pump house.Seat-Puller.jpgSam BarkerEmail hidden; Javascript is required.(304) 629-2284(304) 629-2284Josh FrazierEmail hidden; Javascript is required.(501) 581-1811(501) 581-1811Josh AngelineEmail hidden; Javascript is required.(501) 581-1811(501) 581-1811Josh DaltonEmail hidden; Javascript is required.(724) 825-6859(724) 825-6859Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415Josh Dalton
02/04/201802:30 AMWVBlacksvilleCoastal39deg 41' 42.2"80deg 13' 22.4"1003 Daybrook Rd, Fairview, WV 26570Evening, light snow, 25 degreesCoastal10HBlacksvilleAustin KnowldemProducersShort Service Employee70.51(740) 586-8690

Austin Knowldem was fueling body load frac pump 244

Austin Knowldem was fueling body load frac pump 244, when he made a misstep and fell from the truck. He landed on his hip. Axiom was called and Austin did not seek medical attention. At this time there is no reported injury and no trip to a medical facility.

Matt Umtied

Matt was on the blender when he witnessed Austin fall from the body load frac pump while fueling. He assisted Austin, and it was determined that medical attention was not necessary. Axiom was called. It has been reported that Austin did not seek medical attention.

Limited Visibility, cold weather, light snow, limited oil and gas experienceNNE company man was informed immediately and the incident was reportedA safety meeting was held reminding of the importance of foot placement and having a spotterincident-report1.pdfDan MullinsEmail hidden; Javascript is required.(740) 586-8690(740) 586-8690Ralph BoleyEmail hidden; Javascript is required.(740) 605-4457(740) 605-4457Mike InmanEmail hidden; Javascript is required.(989) 858-6112(989) 858-6112Criss VanGilderEmail hidden; Javascript is required.(405) 757-8725(405) 757-8725Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415Criss VanGilder
10/27/201909:30 AMWVBlacksvilleCumminsN 423926.23E 1776776.64Yank Hollow Road Fairview, WV 26570Cool/showersCummins8HBlacksvilleTravis CasnerComplete EnergyDriver424(304) 514-3726

Loading up Stallion living quarters.

While winching on a stallion living quarters, the dogs on the trucks winch released and allowed the trailer to drop to the ground, trailer fell approximately 1 foot. Inside of living quarters the ceiling tiles fell down and the toilet was shattered and the sink broke.

Travis Casner

While winching up the trailer, the dogs in the main winch released allowing the winch to free spool and the trailer to fall to the ground.

mechanical failureimmediatleyLoad assisted remaining camps with the craneTom PoseyEmail hidden; Javascript is required.(304) 514-3726(304) 514-3726Brent PhillipsEmail hidden; Javascript is required.(740) 502-1218(740) 502-1218Joshua GrimEmail hidden; Javascript is required.(304) 276-3899(304) 276-3899Joshua DaltonEmail hidden; Javascript is required.(724) 825-6859(724) 825-6859Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415
09/13/201909:30 AMWVDaybrookCumminsN 39-39-09.20W 80-12-38.22County Route 25/3 Yank Hollow Road83º SunnyCumminsN/ABlacksvilleDonny KlauseComplete Energy ServicesCrane Operator4310(724) 531-2010

Move crane into position to pick up a load.

Crane moved int position to pick up a load without a spotter. When into position the operator swung crane to the right and struck a parked vehicle with the left corner of it's counter weight.

Scott McDonald

Could hear the crane hit the truck and then seen the Damage.

Operator did not use a spotter as per policy.25 minreview policy regarding crane useTom PhillipsEmail hidden; Javascript is required.(740) 891-8251(304) 368-1384Brent PhillipsEmail hidden; Javascript is required.(740) 502-1218(304) 368-1384Troy HamidiEmail hidden; Javascript is required.(719) 459-2067(719) 459-2067Josh DaltonEmail hidden; Javascript is required.(724) 825-6859(304) 212-0415Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415Troy Hamidi
04/12/202108:50 PMWVFairviewCummins39.66189880.1808911698 Yank Hollow Road, Fairview, WV 26570Cloud CoverCummins14/18BlacksvilleJohnna DickeyGMSGate Guard211(989) 858-6112

Frac Operations. Sand trucks delivering sand to pad

From Mike Inman
Last night around 8:50 PM, I received a text from a Daybrook driver. He asked what was wrong with the female at the lower guard shack. He said that she sounded panicked and had fear in her voice. The roustabout was also down there, he was working on the light plant for the lower guard shack. Ryan with PSC, and myself headed down there. The roustabout was returning to pad, he stopped me, and said that the female guard was scared and was having some issues. We arrived at the guard shack and you could tell she had been crying and was scared. The light plant had tripped out again and the shack had no power. Her boyfriend was also at the shack. I told him to leave and Ryan and myself asked her what was wrong.
She told us that Matt who drives the “Green Weenie” for AEP had caused her issue. She said that he had asked her for a cigarette. He said he would pay for it and she said that it was fine. She went into the shack to get the cigarettes. He came up the window, she handed the cigarette to him through the window. He then grabbed her wrist and said maybe I can fit through the window or something to that affect. She pulled away and said she would slam his hand in the window. Matt then left to go to pad with the load of sand. That is when the light plant died. She had very poor cell service, no CB, and no light. She had called her boyfriend who only was 20 mins away, she also put a crowbar in the shack with her. Matt was then leaving the pipe yard, he pulled up and said I hear you are having CB issues, but since you already have a guy here, I am not going to help you.
We then placed her at the Kassay Pad guard shack, Water transfer has a guy on the Kassay, and the roustabout also stayed at the Kassay pad. She felt safe with that. PSC contacted AEP and told Matt not to return to pad. The AEP dispatcher asked Matt what had happened, Matt said he just asked to buy a cigarette and it must be a conspiracy against him. It was also confirmed that his truck was on the in-out sheet that GMS maintains.
Johnna Dickey has worked for GMS for less than 2 weeks. Her Supervisor is Jeff Weimer at 304-216-7707. Keep in mind that she did not report this because she had only worked there for a short time and was concerned about her job. This was reported to us by other employees looking out for her. I also told her that if she ever felt threatened again, she should immediately drive to pad for help.
Matt Gaynor – driver for AEP. Truck Number #2795. AEP asked that the trailer and box to be dropped at the AEP yard in Washington.

Mike Inman

Last night around 8:50 PM, I received a text from a Daybrook driver. He asked what was wrong with the female at the lower guard shack. He said that she sounded panicked and had fear in her voice. The roustabout was also down there, he was working on the light plant for the lower guard shack. Ryan with PSC, and myself headed down there. The roustabout was returning to pad, he stopped me, and said that the female guard was scared and was having some issues. We arrived at the guard shack and you could tell she had been crying and was scared. The light plant had tripped out again and the shack had no power. Her boyfriend was also at the shack. I told him to leave and Ryan and myself asked her what was wrong.
She told us that Matt who drives the “Green Weenie” for AEP had caused her issue. She said that he had asked her for a cigarette. He said he would pay for it and she said that it was fine. She went into the shack to get the cigarettes. He came up the window, she handed the cigarette to him through the window. He then grabbed her wrist and said maybe I can fit through the window or something to that affect. She pulled away and said she would slam his hand in the window. Matt then left to go to pad with the load of sand. That is when the light plant died. She had very poor cell service, no CB, and no light. She had called her boyfriend who only was 20 mins away, she also put a crowbar in the shack with her. Matt was then leaving the pipe yard, he pulled up and said I hear you are having CB issues, but since you already have a guy here, I am not going to help you.
We then placed her at the Kassay Pad guard shack, Water transfer has a guy on the Kassay, and the roustabout also stayed at the Kassay pad. She felt safe with that. PSC contacted AEP and told Matt not to return to pad. The AEP dispatcher asked Matt what had happened, Matt said he just asked to buy a cigarette and it must be a conspiracy against him. It was also confirmed that his truck was on the in-out sheet that GMS maintains.
Johnna Dickey has worked for GMS for less than 2 weeks. Her Supervisor is Jeff Weimer at 304-216-7707. Keep in mind that she did not report this because she had only worked there for a short time and was concerned about her job. This was reported to us by other employees looking out for her. I also told her that if she ever felt threatened again, she should immediately drive to pad for help.
Matt Gaynor – driver for AEP. Truck Number #2795. AEP asked that the trailer and box to be dropped at the AEP yard in Washington.

Night time, isolated guard shackImmediateDriver was released from serviceCriss VanGilderEmail hidden; Javascript is required.(405) 757-8725(405) 757-8725Andy TravisEmail hidden; Javascript is required.(304) 212-0415(304) 212-0415Mike InmanEmail hidden; Javascript is required.(989) 858-6112(989) 858-6112Mike InmanEmail hidden; Javascript is required.(989) 858-6112(989) 858-6112Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415Criss VanGilder
 Injury Date Injury Time State Township/City Pad Latitude Longitude 911 Address Weather Well Lease Well Number Well Field Personnel/Witness Name Company Position Days Into Hitch Years With Company Years In Oil/Gas Personnel/Wittness Phone Task Summary Witness Name Witness Statement Contributing Factors Notification Timeline Corrective Action Photos & Videos Supervisor Name Supervisor Email Supervisor Phone Supervisor Office Phone HSE Name HSE Email HSE Phone HSE Office Phone Comp. Man Name Comp. Man Email Comp. Man Phone Comp. Man Office Phone NNE Name NNE Email NNE Phone NNE Office Phone NNE HSE Name NNE HSE Email NNE HSE Number NNE HSE Office Phone SUBMITTEE