Injury Date | Injury Time | State | Township/City | Pad | Latitude | Longitude | 911 Address | Weather | Well Lease | Well Number | Well Field | Personnel/Witness Name | Company | Position | Days Into Hitch | Years With Company | Years In Oil/Gas | Personnel/Wittness Phone | Task | Summary | Witness Name | Witness Statement | Contributing Factors | Notification Timeline | Corrective Action | Photos & Videos | Supervisor Name | Supervisor Email | Supervisor Phone | Supervisor Office Phone | HSE Name | HSE Email | HSE Phone | HSE Office Phone | Comp. Man Name | Comp. Man Email | Comp. Man Phone | Comp. Man Office Phone | NNE Name | NNE Email | NNE Phone | NNE Office Phone | NNE HSE Name | NNE HSE Email | NNE HSE Number | NNE HSE Office Phone | SUBMITTEE |
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03/22/2017 | 09:16 PM | WV | Blacksville | I79 south 121 mile post | Blacksville | While driving south on I79 in traffic. A piece of debri struck the windshield of my 2014 f150 on the passenger side causing a chip in the windshield I looked at the vehicles around me and did not notice any vehicles with excessive mud on them | Andy Travis | ||||||||||||||||||||||||||||||||||||||||
04/09/2017 | 08:00 PM | WV | Blacksville | Blacksville | At approximately 1600 PM on 4/9/17, Best Line Equipment rentals was delivering a tele-handler to the Kassay Pad. The driver, Justin, had lowered his drop trailer and unloaded the tele-handler. Justin then attempted to raise his drop trailer. He then noticed the trailer was not working and had released approximately 15-20 gallons of hydraulic fluid onto the Kassay pad. The roustabout also noticed it at the same time and put a duck pond under the trailer. The roustabout continued to contain the hydraulic fluid and the driver reported it to me. We immediately contained with peat moss and began to dig up the fluid and put it a waste dumpster. We have contacted Max with NGE to evaluate the material and the cleanup. I have attached before pictures and we will follow up with after pictures when we can. Non- Hazardous Release (Hydraulic oil approximately 15-20 gallons) | Andy Travis | |||||||||||||||||||||||||||||||||||||||||
04/30/2017 | 01:36 AM | WV | Blacksville | Blacksville | At 21:36 hrs we had an incident while running 5.5 production casing. After latching up a joint of casing on the cat walk with the elevators the Driller began to pick up the joint during that time he floated his elevators back in as normal. At the same time the derrick hand that was operating the cat walk and skate, ran the skate up to far and pushed the joint of casing thru the elevators into the back of the derrick. The driller could not see that the casing had went into the back of the derrick underneath one of the 4X4 beams in the top drive track. The casing struck the beam while coming up and ripped it free from the I beams of the top drive track, the 4X4 beam fell to the floor landing on the rotary table. Kimzy casing crew had 3 men that were working on the floor where the beam fell to the floor, they saw it happen and were able to dive out of the way of the beam before it came to the floor. Myself and the Rig Manager heard the incident happen and immediately went to the rig floor to assess the situation and ensure no one was injured (no injuries). It was found that the top drive track had suffered damage and was bent to the point that the top drive could not come to the floor. (Jay Hewitt was contacted at this time)( Brent Kasmiear Nabors superintendent) We held a safety stand down to allow the personal to calm down and come up with a plan to remove the joint of casing that was still latched in the elevators. Once a plan was in place we removed the joint of casing and rigged down the casing crew and began circulating the casing. | Andy Travis | |||||||||||||||||||||||||||||||||||||||||
05/07/2017 | 11:45 AM | WV | Blacksville | Blacksville | While pressure testing for stage 20 on the Kassay 7H a wing ? on the back of one of the pumps failed catastrophically. Test pressure was 10,657 psig at the time of failure. No one was in the red zone during the incident. | Andy Travis | |||||||||||||||||||||||||||||||||||||||||
06/19/2017 | 04:58 PM | WV | Blacksville | Blacksville | BJ Services employee was performing preventative maintenance on a fluid end. While making the repairs another employee asked him a question, he turned his head to answer the question and the plunger fell and struck him the foot. The injured employee was wearing steel toe/metatarsal boots, but still sustained an injury. The employee was taken to the supervisors truck, Axiom and BJ EHS were notified, first aid and icing the foot were recommended. The employee later decided to have an x-ray 6/22/2017, which revealed a hair line fracture. | Andy Travis | |||||||||||||||||||||||||||||||||||||||||
07/03/2017 | 08:53 PM | WV | Blacksville | Yank Hollow Road Dave Dillie's trailer | Blacksville | I received a complaint from Dave Dillie on July 3,2017. He alleges NNE has caused the floor in his trailer to start to wave, He said he checked the frame, where he could access it with the level, but agreed the frame was level. The allegations started that by drilling under it we changed the water table, which then caused the trailer to settle. After further discussion and the talking through the process of drilling, he claimed it was the sand truck traffic beating on the ground that caused the trailer to settle. I told him I would discuss it with the office and we would get back to him. 7-6-2017 I went out to look at the fence that we needed to reinstall and his daughter asked what we had decided on the trailer. I told her the issue was still being discussed and we would get back to them. Mrs, Dillies cell phone #304-692-5613 | Andy Travis | ||||||||||||||||||||||||||||||||||||||||
08/14/2017 | 07:30 AM | WV | Blacksville | Kassay Pad/DTE Interconnect | Blacksville | DTE's pipeline has a pressure release valve at the interconnect below the Kassay Pad. The valve is set to "pop off" at 1200 psig. Our Kassay pad has a pressure safety high on our pad set at 1150 psig. So, our pad should shut in before the pressure release valve goes off shutting in our pad. The pressure safety high had been disabled and the pressure on the pipleline got above 1200 psig, causing the pressure relief valve to actuate. This venting of gas startled the water truck drivers and they ESD's the pad, which was the correct form of action. Going forward the pressure safety high on the pipeline pressure for the Kassay pad will not be disabled. | Andy Travis | ||||||||||||||||||||||||||||||||||||||||
09/05/2017 | 02:40 PM | WV | Blacksville | Blacksville | A tandem from Lightening trucking was unloading the compressor off the bed, the bridal didn't have enough slack in it so it came off the ear of the skid. When it did the radiator of the compressor was bent. No one was in the red zone and no other equipment was damaged. | Andy Travis | |||||||||||||||||||||||||||||||||||||||||
10/03/2017 | 03:45 PM | WV | Blacksville | Blacksville | I just received word from the field that one of the water truck drivers from Ransom Drilling was killed as a result of his truck wrecking. I?m told as he was traveling on Rt. 50 to/from one the disposal facilities in Ohio, the truck blew a tire and he lost control. DOT is on scene and will conduct an investigation. There is a story already on WBOY?s website with two pictures, as well as WDTV?s website. | Andy Travis | |||||||||||||||||||||||||||||||||||||||||
10/03/2017 | 10:45 PM | WV | Blacksville | Blacksville | At 6:45 pm an Aveda truck driver was unloading his last load of the day unassisted and without authorization. As the pump for the rig was being hoisted up the roller board the line broke dropping the pump approximately 7'. No one was in the area but the pump sustained damage. It bent the skid, which throws the pump out of alignment, damaged the electrical motor and damaged the gear end. It will be about four days before a replacement can be put together. The employee has been terminated for not listening to instructions and going against policies of all three companies involved. After the incident a safety stand down was preformed. | Andy Travis | |||||||||||||||||||||||||||||||||||||||||
10/09/2017 | 05:00 PM | WV | Blacksville | Blacksville | A Day Brook truck hauling fresh water was attempting to pas a parked pickup when it slid off the road. The driver contacted Brad Chadwick and they anchored the truck with a tandem until another water truck could empty it out. Once empty they were able to drive the truck back on the road. The pickup was not supposed to be parked in that location and the Day Brook driver should have not made the attempt with such little clearance. Moving forward we will make sure no one parks along the lease road. | Andy Travis | |||||||||||||||||||||||||||||||||||||||||
10/20/2017 | 11:15 AM | WV | Blacksville | Blacksville | Today at approximately 1115AM a panhandle Casing truck was delivering 9 5/8? casing to the Coastal pad and on his way back through the fisher location, the rear of his trailer hooked the front fender of the Rig Managers truck pushing it into the safety shack. There are no injuries. The Panhandle truck was being driven by Gail See He has been driving tractor trailers since 2002. He is driving out of the Morgantown, WV dispatch phone The red Chevrolet pickup is a Patterson company vehicle driven by Patterson #334 rig manager Jeff Donahue | Andy Travis | |||||||||||||||||||||||||||||||||||||||||
11/13/2017 | 10:30 AM | WV | Blacksville | Blacksville | Kenneth Keeling, a Patterson UTI Motorhand was found passed out under the influence of alcohol in the passenger side front seat of a vehicle on location. Patterson UTI HSE was informed by rig manager Jeff Donahue) and a field sobriety check was performed. Kenneth blew over the legal limit. Patterson was let go and was taken to the airport by Patterson HSE. | Andy Travis | |||||||||||||||||||||||||||||||||||||||||
11/13/2017 | 02:00 PM | WV | Blacksville | Blacksville | Travis was dumping onto the stockpile with A John Deere 250 Artic rock truck. he was slightly downhill, when he dumped the load, the load did not slide out of the truck and it tilted the cab over. there were no injuries and minimal damage to truck. | Andy Travis | |||||||||||||||||||||||||||||||||||||||||
11/15/2017 | 09:30 AM | WV | Blacksville | Blacksville | Ryan Emery from Backwoods Oil & Gas Services, Inc. had to move a light plant from the back of location to the front utiliziing a 12k telehandler. He picked up the light plant with the telehander forks near the back of location. Light plant picked ~2' off the ground. While driving behind the KSW backyard he bumped into Jordan Neville's white F150 with his forks that was parked along the AST containment, damaging the grille and hood. All red zones were in place while equipment was in operation and seat belts were utilized. | Andy Travis | |||||||||||||||||||||||||||||||||||||||||
01/14/2018 | 10:45 PM | WV | Blacksville | Post Frac Move from Campbell Pad to Nine Energy Location | Blacksville | On January 14th at 10:45 PM while moving the Nine Energy grease trailer from the Coastal Pad up the steep hill towards the Fisher Pad, a dash light came on in the Nine Energy pickup truck indicating "Transmission Too Hot" and the engine shut off. The truck began coasting backwards downhill with no steering or brakes. The trailer turned and pulled the pickup into the ditch, then came free from the fifth-wheel ball, which parted the safety chains and the break-away latch. The pickup came to a stop in the ditch, while the trailer continued coasting downhill. The trailer remained upright as it rolled backwards and stopped right before the tree line approximately 70 yds from the lease road. Dustin Merchant was the driver of the Nine Energy pickup. He is a hot shot driver for Nine. He was uninjured, but was taken to the hospital for examination. Dustin also underwent a drug and alcohol test last night and the results were ?negative?. There were no releases involved with the incident. Damage to the pickup includes body damage, driveshaft and possible hidden damage. Damage to the PCE trailer appears to be minor. The trailer has been towed back to the lease road and inspected carefully. Both the truck and trailer have been removed from NNE property. Nine Energy's investigation is ongoing. | Andy Travis | ||||||||||||||||||||||||||||||||||||||||
01/30/2019 | 07:00 AM | WV | Fairmont | NA | 00 | 00 | 000 | Ice | 00 | 00 | Blacksville | Jay Hewitt | NNE | Drilling Manager | 2900 | 8 | 13 | (304) 382-1825 | Driving to work | Came to and intersection and went to stop and slide on ice. Tried to turn the wheel but did not respond. Went through a barb wire fence at 5 mph. | 00 00 | 00 | Ice | 15 min | Take a more traveled road | John Adams | Email hidden; Javascript is required. | (304) 541-5113 | (000) 000-0000 | Andy Travis | Email hidden; Javascript is required. | (304) 951-0909 | (000) 000-0000 | 00 00 | Email hidden; Javascript is required. | (000) 000-0000 | (000) 000-0000 | Jay Hewitt II | Email hidden; Javascript is required. | (304) 382-1825 | (000) 000-0000 | Andy Travis | Email hidden; Javascript is required. | (304) 951-0909 | (304) 212-0415 | ||
02/20/2018 | 09:00 AM | WV | Blacksville | Jenkins | 000 | 000 | 2451 Mason Dixon Hwy, Core, WV 26541 | warm and sunny/clear | Jenkins | 6H | Blacksville | Mitchel Spencer | Patterson UTI | Derricks | 14 | 5 | 5 | (724) 809-6862 | TIH after BHA swap | While tripping in the hole at the beginning of the shift, Mitch was in the derrick, he began to get lightheaded and start to feel unlike himself and was aware enough to stop the job and come down from the derrick once he was able to do so safely. Once on the floor he collapsed but remained conscious, he was then helped down the rig stairs to the rig managers porch were we sat him down on a chair and he began to shake/spasm. Rig manager and myself(Josh Grim) made the call to either take him to the ER or call the ambulance, I decided that I would just take him in my vehicle to the ER since I was familiar with its location. He was then seen by the ER doctor and was instructed to go to the dental complex to be seen, doctor said it was a reaction between the medications that he was previously given for his dental infection. He was prescribed a different medication and we filled it before returning to rig. He is on his last day of his hitch so he will not be working the rest of his shift. | 000 000 | 000 | Prior treatment of dental issues | Co. Man was made aware of the situation and notified supervision as soon as details were made available. | 000 | nne1.png | Troy Hamidi | Email hidden; Javascript is required. | (000) 000-0000 | (724) 249-5027 | 00 00 | Email hidden; Javascript is required. | (000) 000-0000 | (000) 000-0000 | Joshua Grim | Email hidden; Javascript is required. | (304) 276-3899 | (000) 000-0000 | Jay Hewitt | Email hidden; Javascript is required. | (304) 382-1825 | (000) 000-0000 | Andy Travis | Email hidden; Javascript is required. | (304) 951-0909 | (304) 212-0415 | |
09/18/2018 | 12:00 PM | WV | Blacksville | Mepco | 39 39 45.93 | 80 09 07.77 | 579 Mepco Road, Fairview, WV 26570 | Rain overcast | MEPCO | Lease Rd | Blacksville | Michael Knight | Export Fuel | Driver | 5 | 5 | 3 | (724) 610-1532 | Driver had just offloaded fuel on the Mepco pad and was leaving on the lease rd. The driver stated he reached down for his Pepsi and the truck dropped off the left side of the road and bottomed out in the ditch line. Hillbilly towing was called and was able to remove the fueler from the ditch. | Driver had just offloaded fuel on the Mepco pad and was leaving on the lease rd. The driver stated he reached down for his Pepsi and the truck dropped off the left side of the road and bottomed out in the ditch line. Hillbilly towing was called and was able to remove the fueler from the ditch. No injuries, environmental releases, vehicle, or property damage. | Shane Stephenson | Driver had just offloaded fuel on the Mepco pad and was leaving on the lease rd. The driver stated he reached down for his Pepsi and the truck dropped off the left side of the road and bottomed out in the ditch line. Hillbilly towing was called and was able to remove the fueler from the ditch. | Not paying attention | Immediately | Driver will not return to location. Safety meeting was held discussing driver safety | Shane Stephenson | Email hidden; Javascript is required. | (405) 757-8725 | (405) 757-8725 | Shane Stephenson | Email hidden; Javascript is required. | (405) 757-8725 | (405) 757-8725 | Eric Boone | Email hidden; Javascript is required. | (304) 377-6666 | (304) 377-6666 | Andy Travis | Email hidden; Javascript is required. | (304) 951-0909 | (304) 212-0415 | Andy Travis | Email hidden; Javascript is required. | (304) 951-0909 | (304) 212-0415 | Criss VanGilder | |
09/01/2018 | 12:05 AM | WV | Blacksville | Yost | 39.6296 | -80.2149 | 218/Daybrook Run Rd. | 75 deg / Night | Yost | 7H | Blacksville | Charles Fugate | Highlands | Tool Pusher | 5 | 8 | 15 | (304) 890-5197 | Moving center tub out away from the rig. | Charles (Night Tool Pusher) was operating the John Deere front loader to move the center tub away from the rig to pull the HCR off the mud cross. Placed forks underneath the center tub on ODS of the rig. While backing up the front steer tires transitioned from the matting boards to the cellar plates. Deflecting the cellar plates the forks tilted down and slid the center tub off. Tub slid down and pushed the corner of the rig mats into the 5H cage. The impact moved the cellar cage 2' contacting the 2" casing pressure line. Pulled the threads off the 2"nipple between the valve and elbow releasing ~600 psi of pressure. Charles immediately moved the fiberglass cellar cover and closed the valve. | Charles Fugate | While moving the center tub my forks tilted forward after driving onto the cellar plate. Causing the tub to slide off the forks and push the matting boards into the cellar cage. I heard a hissing noise and immediately moved the grating and closed the 2" valve in the cellar. | Driving over cellar with (2) 1/2" cellar plates with a full load. | Tool Pusher notified Ross Drnjevich immediatly after the incedent. | Do not drive over cellars with any equipment. Place equipment between cellars on solid ground. Center tub will be moved one end at a time. | alvin Wilson | Email hidden; Javascript is required. | (304) 539-1883 | (000) 000-0000 | Mike Lawrence | Email hidden; Javascript is required. | (304) 542-8238 | (000) 000-0000 | Ross Drnjevich | Email hidden; Javascript is required. | (724) 579-9683 | (000) 000-0000 | Jay Hewitt | Email hidden; Javascript is required. | (304) 382-1825 | (000) 000-0000 | Andy Travis | Email hidden; Javascript is required. | (304) 951-0909 | (304) 212-0415 | ||
09/11/2018 | 12:20 PM | WV | Morgantown | N/A | 39.634279 | -79.954050 | University Ave | Overcast | N/A | N/A | Blacksville | Andy Travis | NNE | EHS/ Op Ex Coordinator | 2 | 5 | 12 | (304) 951-0909 | While traveling to the field, I was in Morgantown traffic, at a standstill and was rear-ended by a pick up truck. There were no injuries or other parties involved. We pulled off of the busy road and called the police to do an accident report. The other driver was found to be at fault and cited with a warning. Pictures and a copy of the accident investigation report are attached to this report. | Jay Hewitt was a passenger at the time of the incident. | Jay Hewitt | No witness statement | Driver dropped cup and lost focus as a result | Immediate | None | Andy Travis | Email hidden; Javascript is required. | (304) 951-0909 | (304) 212-0415 | Andy Travis | Email hidden; Javascript is required. | (304) 951-0909 | (304) 212-0415 | Andy Travis | Email hidden; Javascript is required. | (304) 951-0909 | (304) 212-0415 | Andy Travis | Email hidden; Javascript is required. | (304) 951-0909 | (304) 212-0415 | Andy Travis | Email hidden; Javascript is required. | (304) 951-0909 | (304) 212-0415 | Andy Travis | |
08/07/2021 | 06:00 AM | WV | Blacksville | ERP | 39.634801 | -80.286653 | 31 Happy Ln Fairview, WV | Clear, warm | ERP | 4H | Blacksville | Josh Angeline | NNE | Consultant | 5 | 1 | 15 | (501) 581-1811 | Loading bha onto catwalk | While loading bha onto catwalk, rig hand backed front end loader into the flange of the flow line causing damage to the rear of the loader | Josh Angeline | While loading bha onto catwalk, rig hand backed front end loader into the flange of the flow line causing damage to the rear of the loader | No spotter was utilized. | Damaged was not reported. Discovered on the next shift. | Utilize a spotter in tight areas of operation | Bobby Gilbert | Email hidden; Javascript is required. | (903) 486-2689 | (903) 486-2689 | Mario Elizondo | Email hidden; Javascript is required. | (878) 218-8696 | (878) 218-8696 | Josh Angeline | Email hidden; Javascript is required. | (501) 581-1811 | (501) 581-1811 | Josh Dalton | Email hidden; Javascript is required. | (724) 825-6859 | (724) 825-6859 | Andy Travis | Email hidden; Javascript is required. | (304) 951-0909 | (304) 212-0415 | Josh Dalton | |
10/08/2020 | 11:45 AM | WV | Fairview | Radiotower | 39.636750 | -80.224431 | Marginal Lane | Sunny/ Clear | n/a | n/a | Blacksville | Michael Shreve | NNE | Contruction Foreman | 4 | 6 | 8 | (304) 918-3050 | Mike went to future Radiotower location to review what timber had been cut. | Walked location, came back to vehicle and ate lunch. Turned on vehicle to leave location and back up into wellhead. Got out of the vehicle to see if there was any damage. The truck tailgate and bumper were damaged, but the well head did not appear to have any damage. Notified Andy Travis of incident and called Daybrook Development, the owner of the well. Day brook inspected the well and said that everything looks to be fine. There were no injuries | n/a n/a | No witnesses were present. | Should have backed into parking spot | Immediate Notification | Back into parking spot, utilize back up camera and mirrors | Dave McDougal | Email hidden; Javascript is required. | (304) 212-0419 | (304) 941-5033 | Andrew Travis | Email hidden; Javascript is required. | (304) 951-0909 | (304) 212-0415 | Dave McDougal | Email hidden; Javascript is required. | (304) 212-0419 | (304) 941-5033 | Dave McDougal | Email hidden; Javascript is required. | (304) 212-0419 | (304) 941-5033 | Andy Travis | Email hidden; Javascript is required. | (304) 951-0909 | (304) 212-0415 | Andy Travis | |
08/28/2018 | 09:15 AM | WV | Blacksville | Yost | 39.641739 | -80.218217 | 3589 Daybrook Rd. Fairview, WV 26570 | Clear and Sunny, Hot | Yost | 7H | Blacksville | will Abraham | Bills Bits | Driver | (412) 518-8405 | Delivering soap tote to location | As the Bill's Bit service driver(William Abraham - (412)518-8405) was pulling onto a congested location, he thought he could squeeze through a tighter spot with his truck and trailer and grazed the bumper of a parked pickup truck belonging to a floorhand(Grover Clawson - (740)434-32432). | 00000 000000 | 000000 | Congested location, impatience/in a hurry | Notified immedietley after everyone was confirmed safe/ok. | Drivers swapped out insurance information and phone numbers. | 00000000000 0000000000 | Email hidden; Javascript is required. | (000) 000-0000 | (000) 000-0000 | 0000000000 000000000000 | Email hidden; Javascript is required. | (000) 000-0000 | (000) 000-0000 | Josh Grim | Email hidden; Javascript is required. | (304) 276-3899 | (000) 000-0000 | Jay Hewitt | Email hidden; Javascript is required. | (304) 382-1825 | (000) 000-0000 | Andy Travis | Email hidden; Javascript is required. | (304) 951-0909 | (304) 212-0415 | |||||
07/01/2021 | 11:05 AM | WV | Blacksville | Lemley | 39.6571144 | 80.1696953 | 781 Long Drain Rd, Fairview, WV 26570 | Partly Sunny | Lemley | 1H | Blacksville | Rob Cowger | NNE | Consultant | 10 | 2 | 25 | (304) 276-2139 | Fracing Stage 42 on the Lemley 1H | During 2.0 lb 100 Mesh on stage 42 on the 1H the turbine caught fire internally. A loud noise was heard from inside the data van, and smoke was seen coming from the turbine. All equipment was immediately shut down. Power Generation also called to shutdown. At this point flames were seen coming from the exhaust of the turbine. Gas supply was shut in, and the 1H and 3H wells were shut in. All nonessential personnel were sent to the muster area, and the onsite NNE consultant called 911 and NNE management. The fire was contained inside the turbine structure, and some small spot fires were visible on the containment from leaking oil. The fire suppression system inside the turbine actuated and smothered the fire internally. The small spot fires were controlled with fire extinguishers. Once the fire department arrived, the fire had already been suppressed. Once the turbine structure cooled to 100 deg F, the fire department opened the turbine doors to confirm the fire was completely out. | Rob Cowger | During 2.0 lb 100 Mesh on stage 42 on the 1H the turbine caught fire internally. A loud noise was heard from inside the data van, and smoke was seen coming from the turbine. All equipment was immediately shut down. Power Generation also called to shutdown. At this point flames were seen coming from the exhaust of the turbine. Gas supply was shut in, and the 1H and 3H wells were shut in. All nonessential personnel were sent to the muster area, and the onsite NNE consultant called 911 and NNE management. The fire was contained inside the turbine structure, and some small spot fires were visible on the containment from leaking oil. The fire suppression system inside the turbine actuated and smothered the fire internally. The small spot fires were controlled with fire extinguishers. Once the fire department arrived, the fire had already been suppressed. Once the turbine structure cooled to 100 deg F, the fire department opened the turbine doors to confirm the fire was completely out. | Investigation Pending | Immediate | Investigation Pending | Criss VanGilder | Email hidden; Javascript is required. | (405) 757-8725 | (405) 757-8725 | Andy Travis | Email hidden; Javascript is required. | (304) 951-0909 | (304) 951-0909 | Rob Cowger | Email hidden; Javascript is required. | (304) 276-2139 | (304) 276-2139 | Criss VanGilder | Email hidden; Javascript is required. | (405) 757-8725 | (405) 757-8725 | Andy Travis | Email hidden; Javascript is required. | (304) 951-0909 | (304) 212-0415 | Criss VanGilder | |
Injury Date | Injury Time | State | Township/City | Pad | Latitude | Longitude | 911 Address | Weather | Well Lease | Well Number | Well Field | Personnel/Witness Name | Company | Position | Days Into Hitch | Years With Company | Years In Oil/Gas | Personnel/Wittness Phone | Task | Summary | Witness Name | Witness Statement | Contributing Factors | Notification Timeline | Corrective Action | Photos & Videos | Supervisor Name | Supervisor Email | Supervisor Phone | Supervisor Office Phone | HSE Name | HSE Email | HSE Phone | HSE Office Phone | Comp. Man Name | Comp. Man Email | Comp. Man Phone | Comp. Man Office Phone | NNE Name | NNE Email | NNE Phone | NNE Office Phone | NNE HSE Name | NNE HSE Email | NNE HSE Number | NNE HSE Office Phone | SUBMITTEE |