Time | State | Township/City | Pad | Latitude | Longitude | 911 Address | Weather | Well Lease | Well # | Well Field | Personnel/Witness Name | Personnel/Wittness Phone | Company | Position | Hitch Days | Years Oil/Gas | Years w/Comp. | Task | Summary | Spill Amount | On containment | Spill contained | NNE Contacted | DEP Contacted | Spill Line Contacted | Notification Timeline | Spill Cleaned Up | Follow Up Required | Corrective Action | Supervisor Name | Supervisor Email | Supervisor Phone | Supervisor Office Phone | Comp. Man Name | Comp. Man Email | Comp. Man Phone | Comp. Man Office Phone | NNE Name | NNE Email | NNE Phone | NNE Office Phone | NNE Name | NNE Email | NNE Phone | NNE Office Phone | NNE HSE Name | NNE HSE Email | NNE HSE Number | NNE HSE Office Phone | SUBMITTEE | |
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04:30 PM | WV | 39.625547 | -79.963157 | Harvey 1 Well | Blacksville | Crude Oil Soil Contamination at the Harvey 1 Well Initial contact made by DEP Inspector, Gayne Knitowski, on March 2nd regarding oil contaminated soil in the immediate area around the wellhead. Also mentioned oil and grease on the wellhead and stuffing box. This was pre-existing condition of the well prior to acquisition by Northeast. Jeremiah Wilt cleaned wellhead and immediate soil area around the wellhead on March 6th. Gayne was notified via email that day with accompanied pictures of site. Gayne re-visited location on March 21st and raised concerns about remaining contaminated soil as well as berm condition of old tanks. He asked that more remediation efforts be done on contaminated soil and repair of tank berm to avoid threat of violation. NGE Environmental onsite morning of the 22nd to obtain samples/pictures of contaminated soil and develop a plan to remediate areas of concern. Plan to pursue tilling of contaminated soil, liming, and re-seed in accordance with regulations. | 5 to 100 gallons | Andy Travis | |||||||||||||||||||||||||||||||||||||||||||
02:00 PM | WV | Produced water hauling | Blacksville | Daybrook Development arrived at the Coastal AST site to offload production water into the Coastal AST. The driver hooked up to the ground manifold and started to pressurize the line, at which point the hose between the truck and the ground manifold failed, specifically at the cam lock connection. Approximately 1 BBL of produced water was sprayed onto the ground, outside secondary containment, but remained on pad. The driver immediately shut the truck off and removed all standing water with the truck. Calls were made to supervisors, as well as the District WV DEP Inspector. NNE's first response environmental clean-up vendor was contacted and dispatched for remediation services. DEP Inspector agreed with NNE's reactionary measures and said there was no need to call WV Spill Hotline. | 5 to 100 gallons | Andy Travis | |||||||||||||||||||||||||||||||||||||||||||||
04:00 PM | WV | Dunkard Creek to Kassay Freshwater Transfer Operations | Blacksville | At approximately 12:00 PM, while crews were transferring freshwater to Dyna Tank #1, the pressure gauge on the booster pump at the Matteo site failed. As a result, approximately 1 gallon of freshwater was released onto the ground, but within the pump's containment. The Rock Water employee manning the pump immediately shut down and notified NNE's Water Consultant. Upon investigation, it was discovered the housing for the stem of the gauge failed, not the gauge itself. Crews replaced same and resumed transferring water. | Less than 1 gallon | Andy Travis | |||||||||||||||||||||||||||||||||||||||||||||
02:15 PM | WV | Coastal Tank Farm | Blacksville | At 10:15 AM, April 3, 2017, NNE found a failure in the tank containment on the Coastal Pad. The failure was a six inch cut in the containment, which allowed standing rain water to exit onto the pad - all water released remained on the pad. Notifications were made, the water was tested and results were within the allowable parameters, a sand bag was placed on top of the cut to reduce any additional water from escaping, and crews were dispatched. Daybrook Development was called to remove all remaining water from containment, and RW Products was called to patch the failed portion of the containment. NNE's WV DEP Inspector was called to provide a summary of the incident, and no further direction was given. | Less than 1 gallon | Andy Travis | |||||||||||||||||||||||||||||||||||||||||||||
04:00 PM | WV | Beach Tank Farm | Blacksville | At 12:00 PM, April 3, 2017, NNE found a failure in the tank containment on the Beach Pad. The failure was a six inch cut in the containment, which allowed standing rain water to exit onto the pad - all water released remained on the pad. Notifications were made, the water was tested and results were within the allowable parameters, a sand bag was placed on top of the cut to reduce any additional water from escaping, and crews were dispatched. Daybrook Development was called to remove all remaining water from containment, and RW Products was called to patch the failed portion of the containment. | Less than 1 gallon | Andy Travis | |||||||||||||||||||||||||||||||||||||||||||||
07:15 PM | WV | Kassay | Blacksville | Per Site Supervisor Glenn Boyd: | 5 to 100 gallons | Andy Travis | |||||||||||||||||||||||||||||||||||||||||||||
05:30 PM | WV | Blacksville | 1-1.5 gallon diesel spill on Statler lease road. Rockwater was moving a fuel cell in place for water transfer from the Statler impoundments. The fuel cell was mostly empty. During transport on the forklift a pump broke off allowing the remaining fuel to spill | 1 to 5 gallons | Andy Travis | ||||||||||||||||||||||||||||||||||||||||||||||
06:45 PM | WV | Fisher | Blacksville | During Line inspections today of the Temp Line Running from Coastal to Fisher location. I found a Diesel Spill coming from a Staged BJ Pump Truck. The Fuel has stoped leaking as of now, the Frac Consultant along with BJ was passed the information. | 5 to 100 gallons | Andy Travis | |||||||||||||||||||||||||||||||||||||||||||||
05:10 PM | WV | Fisher | Blacksville | Have a very small Diesel Spill on the Statler Lease Road. The only Party that looks to be at Fault is Jacobs Fuel. Currently Rock Water is Ordering Clean Up services. | 1 to 5 gallons | Andy Travis | |||||||||||||||||||||||||||||||||||||||||||||
03:45 PM | WV | Water Transfer/ Disposal | Blacksville | I just received word from the field that one of the water truck drivers from Ransom Drilling was killed as a result of his truck wrecking. I?m told as he was traveling on Rt. 50 to/from one the disposal facilities in Ohio, the truck blew a tire and he lost control. DOT is on scene and will conduct an investigation. There is a story already on WBOY?s website with two pictures, as well as WDTV?s website. | 80 bbls | Andy Travis | |||||||||||||||||||||||||||||||||||||||||||||
09:35 PM | WV | Coastal | 39.705903 | -80.203933 | 1001 Daybrook Rd, Fairview WV 26570 | Blacksville | When transporting SBM tank from Fisher to Coastal the truck started down hill and about 1 bbl of SBM splashed out of vent cap on top of tank. It then began to drip down on the lease road. It remained contained to the lease road. | 5 to 100 gallons | Andy Travis | ||||||||||||||||||||||||||||||||||||||||||
03:23 PM | WV | Water Transfer/ Disposal | Blacksville | While performing our bore at the Jakes Run Stream Crossing we have seeped into the stream bed with our drilling mud. The mud finds a way to the surface from the bore. Bentonite is the only foreign substance in the mud. The stream is milky in color. I notified WVDEP inspector. Inspector Arrived on site at 2:10pm | 1 to 5 gallons | Andy Travis | |||||||||||||||||||||||||||||||||||||||||||||
02:00 PM | WV | Coastal | 39.705903 | -80.203933 | 1001 Daybrook Rd, Fairview WV 26570 | Blacksville | While delivering a load of fuel to location, diesel was spotted underneath the fuel truck every time he came to a stop. We followed the truck and immediately got him up on containment and placed a drip pan under the leak. Once the leak was contained we began immediate transfer of fuel from the truck to the diesel tank so we could empty out the fuel load. The drivers name was Rick Bowser (330-847-0087) driving truck #25, He is employed by Mike Ainsley (330-727-1414) of Ainsley oil and has 3 Yrs with the company, 15 years driving experience. | Less than 1 gallon | Andy Travis | ||||||||||||||||||||||||||||||||||||||||||
07:00 PM | WV | Temporary, aboveground waterline between Coastal and Fisher Pads | Blacksville | On 11/21/17 at approximately 4:15 PM and on 11/22/17 at approximately 2:00 PM, as crews were pressure testing the temporary, aboveground waterline between Coastal and Fisher, stress fractures were discovered during the line walks. These fractures allowed freshwater to be released onto the ground. Testing was immediately halted, the line was evacuated, and repairs were made and have been scheduled. The pipe that was delivered for this installation was used previously for other transfer jobs. QAQC was performed on the pipe prior to installation, but due to the nature of these impairments, they could not have been detected until pressure was applied to the line. | 1 to 5 gallons | Andy Travis | |||||||||||||||||||||||||||||||||||||||||||||
08:15 PM | WV | Auxiliary Pad above the Fisher Well Pad | Blacksville | On November 30, 2017 at approximately 3:15 PM, NNE employee arrived onsite at the auxiliary pad above the Fisher Pad and found hydraulic fluid released on the ground where a fusing machine had been sitting. The fusing machine was removed from site, absorbent pads were placed on the contaminated area, and a crew removed the contaminated stone and replaced with clean stone. WV DEP Inspector, Gayne Knitowski, was notified and provided no other action to take. | 1 to 5 gallons | Andy Travis | |||||||||||||||||||||||||||||||||||||||||||||
12:30 PM | WV | Fisher | Blacksville | At 7:30 this morning a 16" temporary above ground waterline owned and operated by Rockwater, parted at a weld during frac operations on the Fisher Pad. The waterline operator had been pumping at 70 bbls/min for a couple of minutes when he noticed a drop in pressure and increase in flow rate. He immediately shut down operations to determine where the potential issue was. The break in the line was found above the Coastal Pad, along the access road that runs between the Fisher and Coastal Pads. We are estimating that 450 bbls of a 30% concentration mixture of produced and fresh water escaped and ran down the hillside and lease road. There are no streams or waterways that connect with the contaminated area. DEP inspector Gayne Knitowski was notifed at 9:00 am this morning, and visited the location. He was supportive of the actions we had taken and asked to be kept in the loop with the NGE plan of action for remediation. DEP spill hotline was contacted at 10:30 am and assigned the following reference number 31-67939. NGE has been brought in to address environmental remediation, and we are scheduling a meeting with Rockwater to address this incident. | 100 gallons or greater | Andy Travis | |||||||||||||||||||||||||||||||||||||||||||||
04:00 PM | WV | Coastal-Campbell Access Road | Blacksville | On 12/13/17 at approximately 11:00 AM, water transfer crew members were relocating a pump from the Campbell Pad to the Dunkard Creek Withdrawal Site and upon transporting the pump, diesel fuel leaked out of the pump's fuel cell in two places along the Coastal-Campbell Access Road. Oil soak rags were immediately placed on the spill areas. The pump was taken to a level area in order to run the pump and use the extra fuel prior to transporting further on uneven terrain and potentially causing further leaking. NNE's HSE Rep and Water Rep talked with crew members about fueling with consideration of transporting pumps. | Environmental > Spill > Petroleum Fuel > 5 to 100 gallons | Andy Travis | |||||||||||||||||||||||||||||||||||||||||||||
06:30 PM | WV | Coastal AST | Blacksville | On 12/13/17 at approximately 1:30 PM, NNE's drilling consultant observed water leaking at a flange on the discharge pipe at the AST. An estimated 2 BBL of blended water was released onto the ground, outside of containment. The water never left the well pad and did not impact any streams. NNE's HSE rep and Water rep went to site to assess situation and put containment under the leak to prevent further spreading. Water transfer crew members were immediately called to break down the flange and identify the failure. Upon breaking the flange down, it was determined the failure was a broken bolt that holds the flange together. Crew members replaced the damaged bolt with a new one, bolted the flange back up, which resolved the issue. | 5 to 100 gallons | Andy Travis | |||||||||||||||||||||||||||||||||||||||||||||
05:00 PM | WV | Fairview | Cummins | N 39-39-09.20 | W 80-12-38.22 | 1698 Yank Hollow Road, Fairview WV 26570 | Rain Showers | Cummins | 10H | Blacksville | Nathan Caldwell | (724) 984-2538 | Northeast Natural Energy | Company man | 8 | 16 | 1 | Was notified of soap suds in run off water believed to be coming off the pad on a neighbors property. Went to investigate. | Upon skidding the rig this morning according to Decker drillings superintendent it is believed that the rig hands disconnected the mist pump lines on the containment. The mist pump lines contained soapy water. We had a torrential downpour. All water went to the back end of our containment which is the lowest point of the burm over flowing into the gravel. The max concentration soap to water is our mist tank is 30 Bbl's of fresh water to 2 gallons off soap. Corrective action was discussed with Deckers superintended, tool pusher and rig crew that anytime lines are disconnected they will be sucked out with the super sucker also additional catch pans will be place under the tote were soap is collected on the the containment. | Less than a gallon | No | NO | Yes | Yes | Yes | Immediately | No | Yes with DEP | Suck out all lines that are disconnected with the super sucker. | Josh Dalton | Email hidden; Javascript is required. | (724) 825-6859 | (304) 212-0424 | Nathan Caldwell | Email hidden; Javascript is required. | (724) 984-2538 | (724) 984-2538 | Andy Travis | Email hidden; Javascript is required. | (304) 951-0909 | (304) 212-0415 | Hollie Medley | Email hidden; Javascript is required. | (304) 543-8932 | (304) 212-0422 | Andy Travis | Email hidden; Javascript is required. | (304) 951-0909 | (304) 212-0415 | ||
12:10 PM | WV | Clay | Yost | 39.6296 | -80.2149 | 000000000000000000 | 00000000000 | Yost | 11H | Blacksville | Josh Grim | (304) 276-3899 | NNE | Companyman | 8 | 18 | 2 | Diesel/water mixture under the mats most likely from an overfill of the boiler. A water truck had split the berming and was allowing the mixture to drip out onto the gravel, gravel was scooped up and disposed of and we began pulling mats to vacuum the liquid out from under them, extreme called out to repair section of containment. | Diesel/water mixture under the mats most likely from an overfill of the boiler. A water truck had split the berming and was allowing the mixture to drip out onto the gravel, gravel was scooped up and disposed of and we began pulling mats to vacuum the liquid out from under them, extreme called out to repair section of containment. | 1-2 gal | No | Yes | Yes | Yes | No | notified immediately | Yes | No | Scratched up gravel, vacuumed under mats. | Josh Grim | Email hidden; Javascript is required. | (304) 276-3899 | (304) 276-3899 | Josh Grim | Email hidden; Javascript is required. | (304) 276-3899 | (304) 276-3899 | Jay Hewitt | Email hidden; Javascript is required. | (304) 382-1825 | (304) 382-1825 | Hollie Medley | Email hidden; Javascript is required. | (304) 543-8932 | (304) 212-0422 | Andy Travis | Email hidden; Javascript is required. | (304) 951-0909 | (304) 212-0415 | ||
07:00 AM | WV | Fairview | McClellan | 39.621619 | 80.278602 | 326 Harvey Run Road | Cloud Cover/Cold | McClellan | 14H | Battelle | Eirc Boone | (304) 377-6666 | NNE | Consultant | 9 | 25 | 3 | Frac McClellan 14H | While performing walk around found approximently 10 gal off road diesel on containment under pump #11 & #13. Spill was cleaned up, leak was found to be coming from braided fuel pump line on pump #11. Pump was shut down and line replaced. Fuel had also breached containment through a bad seam and was trapped between main containment and Felt. Containment was removed, fuel was cleaned up, rock was removed, new felt and containment was laid. | 10 gal | Yes | Yes, but breached containment | Yes | No | No | Immediate | Yes | No | Immediately report all spills | Jim Gallis | Email hidden; Javascript is required. | (740) 252-8508 | (740) 453-9302 | Eric Boone | Email hidden; Javascript is required. | (304) 377-6666 | (304) 377-6666 | Criss Vangilder Criss Vangilder | Email hidden; Javascript is required. | (405) 757-8725 | (405) 757-8725 | Hollie Medley | Email hidden; Javascript is required. | (304) 543-8932 | (304) 212-0422 | Andy Travis | Email hidden; Javascript is required. | (304) 951-0909 | (304) 212-0415 | Criss VanGilder | |
08:00 PM | WV | Fairview | McClellan | 39.621619 | 80.278602 | 326 Harvey Run Road | Snow/Ice | McClellan | 14H | Battelle | Eric Boone | (304) 377-6666 | NNE | Consultant | 9 | 25 | 3 | Frac Operations on the McClellan 6H, 10H, 14H | Following up from prior report from unknown source of spill resulting in spill off containment on 2/10/21 at first was undetermined later was found to be SI SteamStream SC- 405. The leak originated on containment at a camlock on Scale line between scale ISO to blender. The camlock was not secured properly resulting in a slow leak of 600 gal of scale over the course of 12-24 hrs. The scale mixed with snow melt and rain water on containment traveled and collected at the low point of containment berm then leaking through 3 cracked seams in containment breching containment then collecting in standing water off containment. On 2/10/21 containment was cleaned and standing water directly affected off containment was picked up and desposed of in produced water tanks. A sump/trench was cut outside containment to collect and catch any residual that may accumulate. On 2/11/21 another 4-5 gal was picked up with vac truck that had accumulated over the course of 24 hrs. A 40'X70' section of containment was cut out and removed to inspect for any accumulation that could be traped under containment, no accumulation was visibly found. Containment repair replacing the removed section is underway and will be completed before moving removed frac equipment back on. | 600 gal | Yes, but breached | Yes | Eric Boone/Andy Travis/Josh Frazier/Criss Vangilder | Yes | No | Notified at the time of finding/Cleaned up at that time | Yes | Yes, will continue to monitor spill location | Double lock all camlocks with zip ties or duct tape | Criss VanGilder | Email hidden; Javascript is required. | (405) 757-8725 | (405) 757-8725 | Eric Boone | Email hidden; Javascript is required. | (304) 377-6666 | (304) 377-6666 | Andy Travis | Email hidden; Javascript is required. | (304) 951-0909 | (304) 951-0909 | Hollie Medley | Email hidden; Javascript is required. | (304) 543-8932 | (304) 212-0422 | Andy Travis | Email hidden; Javascript is required. | (304) 951-0909 | (304) 212-0415 | Criss VanGilder | |
11:45 AM | WV | Blacksville | Cummins | 39° 36' 54.21"N | 80° 16' 19.02"W | 1698 Yank Yollow Rd | Cold, cloudy, | Cummins | 18H | Blacksville | Rogillo Mandoza | (337) 532-1046 | NOV | operator | 9 | 5 | 5 | Normal solids control operation pumping synthetic based drilling mud into the centrifuge for treatment. | During normal operating conditions, NOV was processing cuttings from the synthetic based drilling mud. A 4" hose that feeds mud into the centrifuge parted. Approximately 5bbls of mud went onto the matting boards below before the operator noticed and shut down the pump. All of the fluid spilled remained on primary containment. The matting boards were picked up and cleaned underneath. The inspector was notified. | 5 bbls | 5 bbls | Yes | Yes | Yes | No | Surface of mats were cleaned immediately. Once daylight the mats were removed to clean under. | Underway | Once rig moves off, all mats will be removed for cleaning. | A strap was added to the hose to remove the stress being placed on it. | Travis Gaspard | Email hidden; Javascript is required. | (337) 254-8556 | (337) 254-8556 | Sam Barker | Email hidden; Javascript is required. | (304) 629-2284 | (304) 629-2284 | Josh Dalton | Email hidden; Javascript is required. | (724) 825-6859 | (724) 825-6859 | Hollie Medley | Email hidden; Javascript is required. | (304) 543-8932 | (304) 212-0422 | Andy Travis | Email hidden; Javascript is required. | (304) 951-0909 | (304) 212-0415 | Josh Dalton | |
05:00 AM | WV | Blacksville | Yost | 39.6296 | -80.2149 | 0000 | 35 degrees clear | Yost | 1H | Blacksville | Devon Runyon | (304) 212-0415 | Precision | Derrickman | 23 | 8 | 0.1 | Moving around immobile equipment in tight space | The Skidsteer was non functional in the front of the drive over. The derrickman attempted to move around the skidsteer with the extend a boom forklift as he needed to get to the other side of location. The rear right tire tagged the 4" mud line going to the drive over causing the hose to separate at the crimped collar causing a 1 to 1-1/2 bbl spill. The ground below and around the spill was excavated to remove all contaminants. | 1-1.5bbl | No | Yes | Yes | Yes | No | 5Min | Yes | No | Safety stand down, put a plan together to clean up area and a solution to prevent the incident in the future. | Troy Holliday | Email hidden; Javascript is required. | (570) 337-3077 | (000) 000-0000 | Troy Hamidi | Email hidden; Javascript is required. | (719) 459-2067 | (000) 000-0000 | Jay Hewitt | Email hidden; Javascript is required. | (304) 382-1825 | (000) 000-0000 | Hollie Medley | Email hidden; Javascript is required. | (304) 543-8932 | (304) 212-0422 | Andy Travis | Email hidden; Javascript is required. | (304) 951-0909 | (304) 212-0415 | ||
06:25 PM | WV | Clay | Mepco | 39.662737 | -80.166485 | 579 Mepco Road, Fairview, WV 26570 | Rainy | Mepco | 2H & 4H | Blacksville | Jeff Wilson | (304) 480-1414 | Solo Construction | Water Consultant | 5 | 25 | 8 | No active task at time of notification of release. | On 9/16/18, at approximately 6:25 PM, NNE was notified by a landowner that water was overflowing an air release valve (ARV) vault and running down the hill. Landowner also notified WV DEP of the incident. NNE made notifications to supervision and dispatched field personnel to visually inspect the site and ensure the leaking had stopped. Once field personnel arrived at ARV site, water was still leaking and detected a one-inch drain valve was open on the bottom of the ARV. The valve was shut and the leaking stopped. Environmental contractor was called to bring erosion controls and gather water and soil samples to begin the remediation process. NNE personnel met with WV DEP Inspector, Gayne Knitowski, to review the site and discuss next steps. Remediation efforts will be ongoing until site is vacant of all contaminated material. Spill hotline was called and NNE was provided reference number 31-80825. | 635 | No | No | Yes | Yes | Yes | 9/16/18, 6:25 PM - Notification of spill; 9/17/18, 10:00 AM - meeting onsite with DEP Inspector; 9/17/18, 3:00 PM - erosion controls installed; 9/18/18, 8:00 AM - water/soil samples gathered | No | Yes | Remediate site until all contaminated materials are removed | Chris Patterson | Email hidden; Javascript is required. | (304) 203-7034 | (304) 212-0417 | Chris Patterson | Email hidden; Javascript is required. | (304) 203-7034 | (304) 212-0417 | Chris Patterson | Email hidden; Javascript is required. | (304) 203-7034 | (304) 212-0417 | Hollie Medley | Email hidden; Javascript is required. | (304) 543-8932 | (304) 212-0422 | Andy Travis | Email hidden; Javascript is required. | (304) 951-0909 | (304) 212-0415 | Chris Patterson | |
Time | State | Township/City | Pad | Latitude | Longitude | 911 Address | Weather | Well Lease | Well # | Well Field | Personnel/Witness Name | Personnel/Wittness Phone | Company | Position | Hitch Days | Years Oil/Gas | Years w/Comp. | Task | Summary | Spill Amount | On containment | Spill contained | NNE Contacted | DEP Contacted | Spill Line Contacted | Notification Timeline | Spill Cleaned Up | Follow Up Required | Corrective Action | Supervisor Name | Supervisor Email | Supervisor Phone | Supervisor Office Phone | Comp. Man Name | Comp. Man Email | Comp. Man Phone | Comp. Man Office Phone | NNE Name | NNE Email | NNE Phone | NNE Office Phone | NNE Name | NNE Email | NNE Phone | NNE Office Phone | NNE HSE Name | NNE HSE Email | NNE HSE Number | NNE HSE Office Phone | SUBMITTEE |