Spill Reports

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 Time State Township/City Pad Latitude Longitude 911 Address Weather Well Lease Well # Well Field Personnel/Witness Name Personnel/Wittness Phone Company Position Hitch Days Years Oil/Gas Years w/Comp. Task Summary Spill Amount On containment Spill contained NNE Contacted DEP Contacted Spill Line Contacted Notification Timeline Spill Cleaned Up Follow Up Required Corrective Action  Supervisor Name Supervisor Email Supervisor Phone Supervisor Office Phone Comp. Man Name Comp. Man Email Comp. Man Phone Comp. Man Office Phone NNE Name NNE Email NNE Phone NNE Office Phone NNE Name NNE Email NNE Phone NNE Office Phone NNE HSE Name NNE HSE Email NNE HSE Number NNE HSE Office Phone SUBMITTEE
01:00 PMWVBlacksvilleBoggess39.67012280.093442030 Mason Dixon Hwy, Maidsville, WV80 deg sunnyBoggess3HBlacksvilleKelby Fowler(304) 377-6666PSCOperator642

Frac Operations Post Blender Swap

Josh Frazier, third party safety, noticed on pad walk around that PSC blender that had been swapped out was parked off containment and leaking water and FR mixture from tub. A total of 5 gal max had leaked out of tub and was under blender.

5 galNoYesYesNoNoImmediateYesNoAll equipment was taken out of service for inspection and repair. No equipment will be left off containmentTony LewellnEmail hidden; Javascript is required.(740) 819-9443(740) 819-9443Eric BooneEmail hidden; Javascript is required.(304) 377-6666(304) 377-6666Criss VanGilderEmail hidden; Javascript is required.(405) 757-8725(405) 757-8725Hollie MedleyEmail hidden; Javascript is required.(304) 543-8932(304) 212-0422Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415Criss VanGilder
04:00 PMWVDaybrookKassayN 39-39-09.20W 80-12-38.22County Route 25/3 Yank Hollow Road98º SunnyKassayN/ABlacksvilleTroy Hamidi(719) 459-2067NNECompany Man8170.75

Rig crew instructed in the morning safety meeting to check equipment that needed to be capped and/or plugged. they men where told where their where caps, plugs and valves opened and to ensure the equipment was ready for transport prior to loading and hauling. The crew failed to ensure that the load and several others where road ready. The result was a 0.5bbl spill from the elk horn from a valve left open. The truck operated by Complete was loaded and hauling to Cummins from Matteo. The NNE company man, noticed drilling fluid along the top left side of the truck bed and wheels. The Company man inspected the truck and then headed up the lease road to find where the spill was located. The company man then took pictures, contacted NNE Drilling Engineer and went to Matteo to speak with the Patterson Rig Manager to make a plan for containment and cleaning.

A 0.5bbl spill occurred just off the Kassay Pad on the lease road heading down hill towards Cummins Pad due to the failure to properly inspect equipment prior to loading. Spill was contained and cleaned up quickly.

0.5 bblnoyesyesnonoimmediateyesnoPatterson Management handling internallyPedro RoblesEmail hidden; Javascript is required.(970) 397-6993(740) 298-9136Troy HamidiEmail hidden; Javascript is required.(719) 459-2067(719) 459-2067Josh DaltonEmail hidden; Javascript is required.(724) 825-6859(724) 825-6859Hollie MedleyEmail hidden; Javascript is required.(304) 543-8932(304) 212-0422Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415Troy Hamidi
10:30 PMWVDaybrook/MonongaliaMatteoN 421911.5E 1771644.925 Yank Hollow Road Fairview, WV 26570ClearMatteo4HBlacksvilleMichael Reed(337) 344-4939NOV SolidsNight shift lead131.5

Drilling operations, normal AFRS operations of backyard equipment running trough, pumps, and centrifuge equipment.

During drilling operations the NOV AFRS system failed to alarm the operators of a high fluid level and go into fail safe shutting down the pumps and flipping the "whale tail". This resulted in the trough overfilling and spilling out over the backside out of view releasing ~20Bbl of OBM onto containment. As soon as run over was spotted system was manually shut down by night shift lead(Michael Reed) and cleanup began.

20BblOn ContainmentYesJosh Dalton/Andy TravisAndy Travis contacted DEPunknownImediatleyEverything that could be cleaned up was moved and cleaned under matting and aboveunknownClean up and reconfigure alarm to sequence auto shutdown.Steven WojoichEmail hidden; Javascript is required.(412) 452-1785(412) 452-1785Joshua GrimEmail hidden; Javascript is required.(304) 276-3899(304) 276-3899Josh DaltonEmail hidden; Javascript is required.(724) 825-6859(724) 825-6859Hollie MedleyEmail hidden; Javascript is required.(304) 543-8932(304) 212-0422Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415
10:30 AMWVBlacksvilleYost39.641639-80.2180563352 Daybrook Road, Fairview, WV 26570SunnyYostASTBlacksvilleMichael Shreve(304) 918-3050NNEConstruction Foreman555

Conducting bi-monthly AST inspection.

While conducting the bi-monthly AST inspection, water was observed to be leaking on the outside of the AST and onto the ground. All water is within the AST's secondary containment and did not leave the site. The cause of the leak is undetermined at this time, until further investigation. The AST will be drained and the liner will be inspected for a failure. Once the failure is located, a repair will be made. If no failure is found, the liner will be replaced in its entirety.

1 - 2 BBLYesYesYesYesNo10:30 AM, M Shreve notified C Patterson. 2:45 PM, C Patterson notified A Travis and G Knitowski (DEP)Not by time of this reportYes, see aboveSee aboveDave McDougalEmail hidden; Javascript is required.(304) 941-5033(304) 212-0419Michael ShreveEmail hidden; Javascript is required.(304) 918-3050(304) 918-3050Chris PattersonEmail hidden; Javascript is required.(304) 203-7034(304) 212-0417Hollie MedleyEmail hidden; Javascript is required.(304) 543-8932(304) 212-0422Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415Chris Patterson
03:07 PMWVBlacksvilleCoastal39.662862-80.2044441001 Daybrook Road, Fairview, WV 26570SunnyCoastalCoastalBlacksvilleBenjamin Musgrave(681) 209-5838NuverraWater Truck Driver58.58.5

Unloading water recovered from drilling from water trucks into AST on Coastal pad.

Driver was unloading when he noticed a leak on the ground. After further investigation, he noticed a wing nut on the truck's pump had broken, allowing the pump to leak. When the leak was discovered, the driver put down absorbent pads and notified his supervisor. Supervisor and HSE rep went to site to conduct clean-up.

1 - 2 gallonsNoYesYesYesNo3:07 PM, spill occurred; 3:16 PM, driver reported to supervisor; 3:57 PM, Nuverra reported to NNE; 4:46 PM, NNE reported to DEP.YesNoCompany has instructed all maintenance crews to check these wing nuts and locking devices for wear and/or cracks and replacing as needed.Donald ReinerEmail hidden; Javascript is required.(304) 594-6066(304) 291-0807Chris PattersonEmail hidden; Javascript is required.(304) 203-7034(304) 212-0417Chris PattersonEmail hidden; Javascript is required.(304) 203-7034(304) 212-0417Hollie MedleyEmail hidden; Javascript is required.(304) 543-8932(304) 212-0422Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415Chris Patterson
05:00 PMWVFairviewCumminsN 39-39-09.20W 80-12-38.221698 Yank Hollow Road, Fairview WV 26570Rain ShowersCummins10HBlacksvilleNathan Caldwell(724) 984-2538Northeast Natural EnergyCompany man8161

Was notified of soap suds in run off water believed to be coming off the pad on a neighbors property. Went to investigate.

Upon skidding the rig this morning according to Decker drillings superintendent it is believed that the rig hands disconnected the mist pump lines on the containment. The mist pump lines contained soapy water. We had a torrential downpour. All water went to the back end of our containment which is the lowest point of the burm over flowing into the gravel. The max concentration soap to water is our mist tank is 30 Bbl's of fresh water to 2 gallons off soap. Corrective action was discussed with Deckers superintended, tool pusher and rig crew that anytime lines are disconnected they will be sucked out with the super sucker also additional catch pans will be place under the tote were soap is collected on the the containment.

Less than a gallonNoNOYesYesYesImmediatelyNoYes with DEPSuck out all lines that are disconnected with the super sucker.Josh DaltonEmail hidden; Javascript is required.(724) 825-6859(304) 212-0424Nathan CaldwellEmail hidden; Javascript is required.(724) 984-2538(724) 984-2538Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415Hollie MedleyEmail hidden; Javascript is required.(304) 543-8932(304) 212-0422Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415
09:00 AMWVMaidsvilleBoggess39.671520-80.0898262030 Mason Dixon Hwy, Maidsville, WV 26541SunnyBoggess5HBlacksvilleJay Hewitt(304) 382-1825Hewitt Energy StrategiesOwner4151

During an inspection of the backyard area, stressed vegetation was noticed on the backside of the Boggess pad. It appeared and was later confirmed that the source of the spill was base oil/drilling mud.

A flow line connecting the mud pits had a slow leak and had been dripping for some time. The location of the line is not readily visible without climbing between the tanks. The entire backyard area is on containment and matted. Unfortunately the leak accumulated over time and found its way under the containment due to a small hole under the matting. I contacted WVDEP, Gayne asked that we get the spill contained to make sure that it does not leave our LOD, and gave us permission for now to continue with drilling operations. Clean up will be done once the rig is moved off of location.

Estimate of 2 bbl spillSpill is outside of containmentSpill has been containedNNE contacted 5/23/2019 at 9:00Gayne Knitowski was contactedNot at this timeImmediate NotificationSpill has not been cleaned upSpill can be cleaned once rig leavesBetter housekeeping around mud pitsJay HewittEmail hidden; Javascript is required.(304) 382-1825(304) 382-1825Troy HamidiEmail hidden; Javascript is required.(719) 459-2067(719) 459-2067Josh DaltonEmail hidden; Javascript is required.(304) 212-0424(304) 212-0424Hollie MedleyEmail hidden; Javascript is required.(304) 543-8932(304) 212-0422Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415Andy Travis
11:15 AMWVMon CountyKassay PadN 39.6583700W 80.1944621190 Yank Hollow Road, Fairview, WV 26570Intermittent RainKassay PadKassay PadBlacksvilleTracy Davis(304) 305-0786Bear ContractingCummins Pad Superintendent30106

Bear Contracting, who is building the Cummins Pad, stores the diesel fuel to refill their equipment on the Kassay Pad in a vessel. (The Cummins Pad entrance begins at the northern end of the Kassay Pad). Woodford, a subcontractor of Bear, was offloading diesel fuel with a fuel truck via hose into the vessel.

Summary of events occurred Monday, April 15, 2019.
Spill Area Approximately 10' by 10', 50 gallons, diesel fuel.
Tracy Davis, Bear Cummins Pad Superintendent, was not on the physical location of the fuel tank. When he contacted me at approximately 12:00 PM he informed me that the truck driver/delivery man for Woodford, a subcontractor of Bear Contracting, had let the on site fuel tank overrun during this mornings fill up. This occurred at approximately 11:15 Am. The secondary containment was either overrun or spray from the full vessel was discharged onto the Kassay well pad outside of the secondary containment for the vessel . (Visual estimation of 50 gallons). It is not known how much freeboard was available in the secondary containment prior to incident. It is believed that no fuels left the Kassay Well Pad containment per Tracy Davis. Mr. Davis indicted the driver for Woodford was not cooperative in providing any information regarding the incident. Mr. Davis is to provide a detailed report via email. Also, NNE employee Jeff Wilson, was on location during the incident. Please see Mr. Wilson's comments regarding the incident via email attachment. Also see photos post incident provided by Mr. Davis.

50 gallons +-Secondary containment around vessel breached. Contained on Kassay well Pad.YesYesnonoWithin 15 minutes of incidentOngoingYesNNE notifed, oil rags and booms placed.Mark UrsoEmail hidden; Javascript is required.(304) 677-2195(304) 326-0160Tracy DavisEmail hidden; Javascript is required.(304) 305-0786(304) 326-0160Dave McDougalEmail hidden; Javascript is required.(304) 941-5033(304) 212-0419Hollie MedleyEmail hidden; Javascript is required.(304) 543-8932(304) 212-0422Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415Dave McDougal
12:10 PMWVClayYost39.6296-80.214900000000000000000000000000000Yost11HBlacksvilleJosh Grim(304) 276-3899NNECompanyman8182

Diesel/water mixture under the mats most likely from an overfill of the boiler. A water truck had split the berming and was allowing the mixture to drip out onto the gravel, gravel was scooped up and disposed of and we began pulling mats to vacuum the liquid out from under them, extreme called out to repair section of containment.

Diesel/water mixture under the mats most likely from an overfill of the boiler. A water truck had split the berming and was allowing the mixture to drip out onto the gravel, gravel was scooped up and disposed of and we began pulling mats to vacuum the liquid out from under them, extreme called out to repair section of containment.

1-2 galNoYesYesYesNonotified immediatelyYesNoScratched up gravel, vacuumed under mats.Josh GrimEmail hidden; Javascript is required.(304) 276-3899(304) 276-3899Josh GrimEmail hidden; Javascript is required.(304) 276-3899(304) 276-3899Jay HewittEmail hidden; Javascript is required.(304) 382-1825(304) 382-1825Hollie MedleyEmail hidden; Javascript is required.(304) 543-8932(304) 212-0422Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415
02:00 PMWVBlacksvilleCoastal39.705639-80.2044441001 Daybrook Road, Fairview, WV 26570SunnyCoastalASTBlacksvilleBronson Martin(702) 904-4301Comtech Inudstries, Inc.Laborer11.51.5

Re-fueling a portable heater unit.

"While re-fueling a third piece of equipment (a portable heater unit) the transfer / pump hose split and began to spray / release diesel fuel. The employee immediately shut down the pump and began to place spill pads to absorb the fuel. The fuel was on the bed of the truck as well as on the ground. Before the truck was moved it was cleaned to verify no additional areas would be affected. Approximately 2 - 4 gallons of diesel fuel was released (see attached photos). The spill area was cleaned up by placing the soiled spill pads and any dirt / rocks, that were affected, into collection buckets for disposal. The hose transfer line on the fuel cell was immediately replaced."

2 - 4 gallonsNoYesYesNoNo2:00 PM - spill occurred; 2:43 PM - Comtech notified NNEYesNoReplaced split / failed hose on the transfer pump of the fuel cell; modify inspection procedure of fuel cell to include routine replacement of the transfer hose (at least every 6 months).Levi BristorEmail hidden; Javascript is required.(724) 263-0105(724) 263-0105Anthony CarlsonEmail hidden; Javascript is required.(304) 216-8886(304) 216-8886Chris PattersonEmail hidden; Javascript is required.(304) 203-7034(304) 212-0417Hollie MedleyEmail hidden; Javascript is required.(304) 543-8932(304) 212-0422Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415Chris Patterson
05:00 AMWVBlacksvilleYost39.6296-80.2149000035 degrees clearYost1HBlacksvilleDevon Runyon(304) 212-0415PrecisionDerrickman2380.1

Moving around immobile equipment in tight space

The Skidsteer was non functional in the front of the drive over. The derrickman attempted to move around the skidsteer with the extend a boom forklift as he needed to get to the other side of location. The rear right tire tagged the 4" mud line going to the drive over causing the hose to separate at the crimped collar causing a 1 to 1-1/2 bbl spill. The ground below and around the spill was excavated to remove all contaminants.

1-1.5bblNoYesYesYesNo5MinYesNoSafety stand down, put a plan together to clean up area and a solution to prevent the incident in the future.Troy HollidayEmail hidden; Javascript is required.(570) 337-3077(000) 000-0000Troy HamidiEmail hidden; Javascript is required.(719) 459-2067(000) 000-0000Jay HewittEmail hidden; Javascript is required.(304) 382-1825(000) 000-0000Hollie MedleyEmail hidden; Javascript is required.(304) 543-8932(304) 212-0422Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415
12:45 PMWVMonongalia CountyCoastal39.705639-80.2044441001 Daybrook Road, Fairview, WV 26570OvercastCoastalCoastalBlacksvilleJosh Null(304) 599-8384RW ProductsManager266

Crew was on the Coastal Pad removing solids from the AST, loading into vac boxes, and making ready for transport to disposal.

After the solids removal crew loaded one of the vac boxes, it was relocated from the work area to the staging area to wait for transport to disposal. As it was being unloaded from the roll-off truck to the staging area, the hatch door wasn't fully closed and allowed some of the solids/sludge to escape and spill onto the pad, outside secondary containment. The solids removal crew cleaned up the sludge and dressed in the area with new stone.

5 gallonsNoYesYesNoNo01/07/19, 12:45 PM - Notified of spillYesNoEnsure all doors on vac boxes are shut and fully bound with chain binders; incorporate into JSAs going forward.Pat JusticeEmail hidden; Javascript is required.(681) 285-5040(304) 277-1110Jeff WilsonEmail hidden; Javascript is required.(304) 480-1414(304) 480-1414Chris PattersonEmail hidden; Javascript is required.(304) 203-7034(304) 212-0417Hollie MedleyEmail hidden; Javascript is required.(304) 543-8932(304) 212-0422Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415Chris Patterson
01:00 PMWVGrant Dist., Monongalia Co.N/A39.615723-80.089051N/AOvercastMichaelMon River WaterlineBlacksvilleAnthony Carlson(304) 216-8886Solo ConstructionWater Consultant7108

Following up on notification that a diesel spill had occurred at the Booster #2 pump station on the Mon River Waterline.

On 03 Jan 19, at approximately 1:00 PM, a diesel spill was discovered at Booster #2 pump station on the Mon River Waterline, outside secondary containment and estimated to be 5 gallons. No waters of the state or US were affected. It was determined this occurred near the end of the last transfer activity and went unreported. After discovery, a crew was dispatched to remove the contaminated stone and replace with new stone. The Spill Hotline was called and provided the following reference number: 31-84925. DEP Waste and Water Inspector Travis Hayes is also aware of the spill and the remedial actions taken.

5 gallonsNoYesYesYesYes01/03/19, 1 PM - Spill Discovery & DEP notification; 4:30 PM - Spill HotlineYesYesRemoved contaminated stone and replaced with new stoneCasey BuckhananEmail hidden; Javascript is required.(304) 224-5567(304) 224-5567Anthony CarlsonEmail hidden; Javascript is required.(304) 216-8886(304) 216-8886Chris PattersonEmail hidden; Javascript is required.(304) 203-7034(304) 212-0417Hollie MedleyEmail hidden; Javascript is required.(304) 543-8932(304) 212-0422Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415Chris Patterson
08:00 AMWVBlBeachNANANAcold/icyBeachBeach PadBlacksvilleDavid Beckner(304) 380-7133NNEWell Tender36511

Operations of Wells

Daybrook was filling the heater with fuel and overfilled heater causing fuel to spill on ground.

5 gallonsnoyesyesyesnoimmediatelyin processnoCleaned upJohn LandisEmail hidden; Javascript is required.(304) 216-6854(304) 212-0434David BecknerEmail hidden; Javascript is required.(304) 380-7133(304) 212-0426John LandisEmail hidden; Javascript is required.(304) 216-6854(304) 212-0434Hollie MedleyEmail hidden; Javascript is required.(304) 543-8932(304) 212-0422Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415John Landis
06:00 AMWVBlacksvilleCampbellNANANAcold/icyCampbell6HBlacksvilleDavid Beckner(304) 380-7133NNEWell Tender311

Operations of Wells

The Campbell 6H was down and when checked on found that the dump valve had blown out. This caused produced water to flow out in Unit and on to ground.

2bblsnoyesyesnonoimmediatelyyesnoCleaned upJohn LandisEmail hidden; Javascript is required.(304) 216-6854(304) 212-0434David BecknerEmail hidden; Javascript is required.(304) 380-7133(304) 212-0426John LandisEmail hidden; Javascript is required.(304) 216-6854(304) 212-0434Hollie MedleyEmail hidden; Javascript is required.(304) 543-8932(304) 212-0422Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415John Landis
06:25 PMWVClayMepco39.662737-80.166485579 Mepco Road, Fairview, WV 26570RainyMepco2H & 4HBlacksvilleJeff Wilson(304) 480-1414Solo ConstructionWater Consultant5258

No active task at time of notification of release.

On 9/16/18, at approximately 6:25 PM, NNE was notified by a landowner that water was overflowing an air release valve (ARV) vault and running down the hill. Landowner also notified WV DEP of the incident. NNE made notifications to supervision and dispatched field personnel to visually inspect the site and ensure the leaking had stopped. Once field personnel arrived at ARV site, water was still leaking and detected a one-inch drain valve was open on the bottom of the ARV. The valve was shut and the leaking stopped. Environmental contractor was called to bring erosion controls and gather water and soil samples to begin the remediation process. NNE personnel met with WV DEP Inspector, Gayne Knitowski, to review the site and discuss next steps. Remediation efforts will be ongoing until site is vacant of all contaminated material. Spill hotline was called and NNE was provided reference number 31-80825.

635NoNoYesYesYes9/16/18, 6:25 PM - Notification of spill; 9/17/18, 10:00 AM - meeting onsite with DEP Inspector; 9/17/18, 3:00 PM - erosion controls installed; 9/18/18, 8:00 AM - water/soil samples gatheredNoYesRemediate site until all contaminated materials are removedChris PattersonEmail hidden; Javascript is required.(304) 203-7034(304) 212-0417Chris PattersonEmail hidden; Javascript is required.(304) 203-7034(304) 212-0417Chris PattersonEmail hidden; Javascript is required.(304) 203-7034(304) 212-0417Hollie MedleyEmail hidden; Javascript is required.(304) 543-8932(304) 212-0422Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415Chris Patterson
11:30 AMWVMaidsvilleJenkins39.711342°-80.139292°3835 Mason Dixon Hwy, Maidsville WV 26541SunnyJenkinsRig MoveBlacksvilleJosh Frazier(304) 517-6188NE Safety SolutionsSafety Consultant2101

While performing a site inspection, Josh Frazier noticed that there was a track of fluid spilled onto the Jenkins location road staging area.

After the rig move, Josh Frazier pulled onto location to perform a safety check and noticed a track of fluid where we had staged some of the Patterson equipment for the move, He notified supervision which in turn notified NNE Compnayman Josh Grim. Josh went out to check the area and get Chisler Brothers out to perform the clean up. By the time I had reached the location Chisler was already there and had absorbant on the spill and were prepping to scrape up any contamination and haul it off to be disposed of.

Less than one gallonSpill was off containment on gravel staging areaThe spill area was limited to the staging areaJosh Frazier notified as soon as spill was discoveredDEP inspector Gayne Knitowski was notified by voicemailSpill line has not been contactedNotification came from random safety inspectionSpill cleaned upNo follow up requiredNeed to do site inspection after moveJosh GrimEmail hidden; Javascript is required.(304) 276-3899(304) 276-3899Josh GrimEmail hidden; Javascript is required.(304) 276-3899(304) 276-3899Jay HewittEmail hidden; Javascript is required.(304) 382-1825(304) 382-1825Hollie MedleyEmail hidden; Javascript is required.(304) 543-8932(304) 212-0422Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415Andy Travis
01:00 PMWVFairviewFisher/Coastal/Campbell access road39.694428°-80.221339°1003 Daybrook RdPartly CloudyFishern/aBlacksvilleAndy Travis(304) 951-0909NNEHSE Coordinator2114

While conducting a field review I noticed a spill on the access road. I contacted Chris Patterson to check on any reported water truck spills. The majority of the traffic at this time is water trucks moving water from the Fisher pad, and DTE coopers run facility upgrade. Chris checked with the field coordinators, and received 2 conflicting reports claiming to have witnessed the spill. One report from ECM claimed that a Daybrook water truck leaked the fluid, and the other Report from Ransom claimed that a truck hauling a gooseneck trailer spilled the fluid. The spilled substance had a petroleum odor, but was green in appearance, could have been oil or a mixture.

Mike Shreve called out Chisler Brothers to cleanup contaminated materials , and replace with fresh gravel. Cleanup was completed within 2 hours of finding spill.

1 gallon or lessNot on containmentSpill was limited to access roadNNE was not notifiedCalled spill into WVDEP inspector Gayne KnitkowskiNot required to be reported through spill hotlineNNE was not notified of spillSpill cleaned up (1 hour)No follow up required for spillStress the importance of reporting in safety meetingsAndy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415Hollie MedleyEmail hidden; Javascript is required.(304) 543-8932(304) 212-0422Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415Andy Travis
09:50 AMWVblacksvilleCoastal39 41 42.280 13 22.41003 Daybrook Road, Fairview, WV 26570cloudy, 40 degreesCoastal4BlacksvilleMax Oliver(817) 526-4147NNEConsultant20407

Performing a pad walk around. The vacuum truck personnel reported a diesel spill on pad where personnel vehicles park.

The vacuum truck guys just reported a fuel spill in the “parking area’. This area is usually crowded with vehicles, especially at crew change. Needless to say, no one will admit to the spill. I estimate probably 3-6 gallons. The way the fuel ran, I think someone was back in parked there with either a “drop tank” or a 5 gallon type can. I think it happened after crew change, no fuel was tracked off of location.

The source of the spill is unknown at this time. The spill was cleaned up and contained. The contaminated gravel and soil has been picked up and disposed of in the environmental dumpster.

4 galNoYesYesYesNoImmediatelyYesNoThe source of the spill is unknown at this time. The spill was cleaned up and contained. The contaminated gravel and soil has been picked up and disposed of in the environmental dumpster.diesel-spill.jpgMax OliverEmail hidden; Javascript is required.(817) 526-4147(817) 526-4147Max OliverEmail hidden; Javascript is required.(817) 526-4147(817) 526-4147Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415Hollie MedleyEmail hidden; Javascript is required.(304) 543-8932(304) 212-0422Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415Criss VanGilder
08:30 PMWVblacksvilleCoastal39 41 42.280 13 22.41003 Daybrook Road, Fairview, WV 2657031 deg, Cloudy, DarkCoastal4BlacksvilleWilliam Miller(989) 858-6112Rock WaterFuel Hauler552

Hauling Fuel

At approximately 8:30 PM, Rock water’s fuel truck reported seeing a fuel spill on the lease road by the county road. The release was just uphill from the county road, which would be on the Coastal side. The roustabout went there immediately to evaluate the situation. The roustabout returned and gathered material to contain the unintended release. Peat Moss and oil soak rags were placed to contain the fuel. I estimate that the release was under 5 gallons. Producers had just received a delivery from Stewart Oil. The fuel delivery truck off loaded, there was a Producers employee watching and assisting the driver. There were no issues during or immediately after the delivery. Producers field supervisor called the delivery driver and asked him if he had an unintended release. The driver stated that he did not believe so but would pull over and inspect his truck. The Fuel delivery driver did call back and stated that his lower vapor line cap was off. He also stated that the vapor line will sometimes collect a little fuel when he off loads a load of fuel. The driver also states that the cap was on when he did a pre-trip prior to leaving. Steward oil also said that they will utilize a trailer that does not have a lower vapor line from now on.
The release of fuel was cleaned up by Producers employees and the roustabout. They used an excavator and shovels to scrap the area. Peat moss was also utilized to help in the collection. Fresh gravel was also replaced on the lease road. Producers supervisor and the roustabout said that all the fuel was collected, and the area looked good. I will also inspect the area in the morning. The poly line was spray painted with orange to identify the area for future inspections. The waste was placed in a leak proof container and returned to the Coastal pad for proper disposal.
I personally thanked the Rock Water driver for reporting the incident which allowed us to begin the clean up immediately. The driver also states that the fuel truck was ahead of him on the lease road. This allowed us to have a very accurate time line for the release. Producers also thanked the fuel delivery truck driver for his honesty about the vapor cap missing.
Time of day: 20:30 on March 2, 2018.
Temperature: 31 Degs
Material released: On road diesel fuel
Wind: Calm
Delivery Truck info: Stuart Oil out of Parkersburg, WV
Driver: Eric Stuart (304) 482-1179
I have also attached 2 photos. The one picture shows a lot of peat moss. You can also see that it is mostly dry which means that there was not much fuel to absorb.

5 galNoYesYesYesNoImmediatelyYesNoThe release of fuel was cleaned up by Producers employees and the roustabout. They used an excavator and shovels to scrap the area. Peat moss was also utilized to help in the collection. Fresh gravel was also replaced on the lease road. Producers supervisor and the roustabout said that all the fuel was collected, and the area looked good. I will also inspect the area in the morning. The poly line was spray painted with orange to identify the area for future inspections. The waste was placed in a leak proof container and returned to the Coastal pad for proper disposal. I personally thanked the Rock Water driver for reporting the incident which allowed us to begin the clean up immediately. The driver also states that the fuel truck was ahead of him on the lease road. This allowed us to have a very accurate time line for the release. Producers also thanked the fuel delivery truck driver for his honesty about the vapor cap missing.Eric StuartEmail hidden; Javascript is required.(304) 482-1179(304) 482-1179Mike InmanEmail hidden; Javascript is required.(989) 858-6112(989) 858-6112Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 951-0909Hollie MedleyEmail hidden; Javascript is required.(304) 543-8932(304) 212-0422Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415Criss VanGilder
10:30 AMWVFairviewCoastal39.705903-80.2039331001 Daybrook Rd, Fairview WV 26570SunnyCoastal6HBlacksvilleMax Oliver(817) 526-4147ARCFrac Consultant45387

As we finished Coastal 6H stg 13, one of the hands called on the radio to tell us there was an FR spill. Went back and checked, a load of FR was delivered during the stage, the driver was told not to blow off until we were finished. (it causes the FR pumps to lose prime). Evidently, he left the pump running and left. I don’t know where he went. When the Producers guys found it there was a large quantity of FR on the containment, pumps, pump room and a small amount beside the containment. There is even a thin film on the side of the AST.

Driver – Richard Charles says he owns Charco Three the trucking company. Truck Tag AG 68768 Pennsylvania Trailer Tag PT 672E2, Copy of CDL attached, did not have any proof of insurance
Hauling for – Flowtek (FR supplier)

When asked why he was pumping after being told not to pump, he claimed no one told him. I believe this statement to be an absolute untruth. I asked him his name, I asked his employer and he told me Flowtek, I asked for his supervisors number and he gave me Rick Shaner 412-452-4032. I called Rick and found out Richard doesn’t work for Flowtek. I doubt almost everything the guy has told me.
It appears Richard Charles owns Charco Three (trucking company) and is self-employed.
Richard was told not to leave the pad until Producers was through with their investigation, he tried to get up the hill 3 times, powering out each time, before Producers employees got him stopped and backed off the hill.

The estimated volume at this time is 100 gallons until we know better. (really hard to tell how much some is on top of pumps.

We have captured as much as we can off of containment, cut the saturated felt up. The small amount off containment has been soaked with moss and will be picked up and contained. The containment is being cut out and repaired were it is soaked.

Hopefully, we will be back in operation within the next hour or two, as soon as the mat is repaired and the trucks re-spotted.

300 Gallons298 GallonsSpill was containedContacted Criss VanGuilderGayne KnitowskiNot Req2 hrsSpill Cleaned (6 hours)NonePendingShane StephensonEmail hidden; Javascript is required.(740) 586-8729(740) 454-6253Max OliverEmail hidden; Javascript is required.(817) 526-4147(817) 526-4147Criss VanGuilderEmail hidden; Javascript is required.(405) 757-8725(304) 212-0423Hollie MedleyEmail hidden; Javascript is required.(304) 543-8932(304) 212-0422Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415Andy Travis
03:07 PMWVFairviewMcClellan39.6219724-80.2741675326 Harvey Run RdSunny/ ClearMcClellan5H, 9H, 13H & 17HBattelleDeshawn Holyfield(412) 443-0741Select Energy ServicesLaborer400

Transferring produced water from the ASTs on the McClellan pad to the frac tank on the McClellan staging area in order to load out trucks.

AT APPROXIMATELY 3:07PM, ON APRIL 2, 2021, NNE WAS NOTIFIED THAT THE FRAC TANK AT THE MCCLELLAN STAGING AREA WAS OVERFLOWING. THE SELECT ENERGY SERVICES ("SES") HAND THAT WAS SUPPOSED TO BE OVERSEEING THE PUMPING AND TANK FILLING WAS DISTRACTED BY HIS PHONE AND ALLOWED THE TANK TO OVERFLOW. PRODUCED WATER WAS PUMPED INTO THE TANK TO THE POINT THAT THE TANK ITSELF OVERFLOWED INTO THE SECONDARY CONTAINMENT, THEN BREACHED THE SECONDARY CONTAINMENT AND WAS RELEASED ONTO THE GROUND, AN ESTIMATED 50 BBL WAS RELEASED ONTO THE GROUND. THE PUMP WAS IMMEDIATELY SHUT DOWN TO ELIMINATE THE SOURCE. WATER TRUCKS WERE DISPATCHED IMMEDIATELY TO EVACUATE ALL WATER FROM THE SECONDARY CONTAINMENT AND GROUND. E & S CONTROLS WERE PLACED IN ORDER TO MINIMIZE IMPACTS AND PREVENT FURTHER CONTAMINATION. NO STREAMS OR WETLANDS WERE AFFECTED BY THE SPILL. SES DISPATCHED MCCUTCHEON, AN ENVIRONMENTAL CLEAN-UP CREW, TO FULLY ADDRESS THE SPILL AREA. THE WV DEP INSPECTOR, BRYAN HARRIS, WAS NOTIFIED, AS WELL AS THE SPILL HOTLINE (REFERENCE ID 31-13410). MR. HARRIS VISITED THE SITE AND WAS HAPPY WITH THE STEPS TAKEN AND PLAN AHEAD. SES WILL BE COMPLETING A SPILL REPORT AND WILL SUBMIT.

50 BBLNoSpill has been containedYesYesYes15:07 - NNE notified of spill; 15:33 - NNE EH&S notified; 15:37 - WV DEP Inspector notified (VM); 17:11 - WV DEP Inspector confirmed; 18:29 - WV Spill Hotline notified.In progress as of 19:50SES will follow up with spill reportSES employee terminated from this NNE site as well as any othersMicah KrafEmail hidden; Javascript is required.(412) 614-9646(412) 443-0741Anthony CarlsonEmail hidden; Javascript is required.(304) 216-8886(304) 216-8886Chris PattersonEmail hidden; Javascript is required.(304) 203-7034(304) 212-0417Hollie MedleyEmail hidden; Javascript is required.(304) 543-8932(304) 212-0422Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415Andy Travis
07:00 AMWVFairviewMcClellan39.62161980.278602326 Harvey Run RoadCloud Cover/ColdMcClellan14HBattelleEirc Boone(304) 377-6666NNEConsultant9253

Frac McClellan 14H

While performing walk around found approximently 10 gal off road diesel on containment under pump #11 & #13. Spill was cleaned up, leak was found to be coming from braided fuel pump line on pump #11. Pump was shut down and line replaced. Fuel had also breached containment through a bad seam and was trapped between main containment and Felt. Containment was removed, fuel was cleaned up, rock was removed, new felt and containment was laid.

10 galYesYes, but breached containmentYesNoNoImmediateYesNoImmediately report all spillsJim GallisEmail hidden; Javascript is required.(740) 252-8508(740) 453-9302Eric BooneEmail hidden; Javascript is required.(304) 377-6666(304) 377-6666Criss Vangilder Criss VangilderEmail hidden; Javascript is required.(405) 757-8725(405) 757-8725Hollie MedleyEmail hidden; Javascript is required.(304) 543-8932(304) 212-0422Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415Criss VanGilder
08:00 PMWVFairviewMcClellan39.62161980.278602326 Harvey Run RoadSnow/IceMcClellan14HBattelleEric Boone(304) 377-6666NNEConsultant9253

Frac Operations on the McClellan 6H, 10H, 14H

Following up from prior report from unknown source of spill resulting in spill off containment on 2/10/21 at first was undetermined later was found to be SI SteamStream SC- 405. The leak originated on containment at a camlock on Scale line between scale ISO to blender. The camlock was not secured properly resulting in a slow leak of 600 gal of scale over the course of 12-24 hrs. The scale mixed with snow melt and rain water on containment traveled and collected at the low point of containment berm then leaking through 3 cracked seams in containment breching containment then collecting in standing water off containment. On 2/10/21 containment was cleaned and standing water directly affected off containment was picked up and desposed of in produced water tanks. A sump/trench was cut outside containment to collect and catch any residual that may accumulate. On 2/11/21 another 4-5 gal was picked up with vac truck that had accumulated over the course of 24 hrs. A 40'X70' section of containment was cut out and removed to inspect for any accumulation that could be traped under containment, no accumulation was visibly found. Containment repair replacing the removed section is underway and will be completed before moving removed frac equipment back on.

600 galYes, but breachedYesEric Boone/Andy Travis/Josh Frazier/Criss VangilderYesNoNotified at the time of finding/Cleaned up at that timeYesYes, will continue to monitor spill locationDouble lock all camlocks with zip ties or duct tapeCriss VanGilderEmail hidden; Javascript is required.(405) 757-8725(405) 757-8725Eric BooneEmail hidden; Javascript is required.(304) 377-6666(304) 377-6666Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 951-0909Hollie MedleyEmail hidden; Javascript is required.(304) 543-8932(304) 212-0422Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415Criss VanGilder
11:10 AMWVFairviewCummins1776892.4423957.932575 Daybrook Rd. Fairview, WV 2657040º / çloudyCummins6HBlacksvilleReggie Neil(234) 855-5874CS TruckingDriver1107

Delivering base oil to the Cummins Pad

While delivering base oil to the HZ rig on the Cummins pad, the truck blew a radiator hose traveling inbound to the Matteo/Kassay/Cummins pads. As he reached the hilltop, he saw steam coming from under the hood. The driver continued up the hill to a safe spot to pull over just before the Matteo Pad next to the guard shack. The driver used absorbent pads to clean up the radiator fluid. Company man made several passes up and down the road searching for any additional spillage but was unable to locate any. Company man had driver back up truck, place new absorbent pads underneath, cleaned up all radiator fluid on ground, and the driver waited for mechanic to arrive to do repairs. Less than 1 gallon was visibly on the ground and was immediately cleaned up.

less than 1 gallonnonoYesNoNoImmediatelyYesNoneNonePedro RoblesEmail hidden; Javascript is required.(770) 894-3276(770) 894-3276Troy HamidiEmail hidden; Javascript is required.(304) 629-2284(304) 629-2284Josh DaltonEmail hidden; Javascript is required.(724) 825-6859(724) 825-6859Hollie MedleyEmail hidden; Javascript is required.(304) 543-8932(304) 212-0422Andy TravisEmail hidden; Javascript is required.(304) 951-0909(304) 212-0415Josh Dalton
 Time State Township/City Pad Latitude Longitude 911 Address Weather Well Lease Well # Well Field Personnel/Witness Name Personnel/Wittness Phone Company Position Hitch Days Years Oil/Gas Years w/Comp. Task Summary Spill Amount On containment Spill contained NNE Contacted DEP Contacted Spill Line Contacted Notification Timeline Spill Cleaned Up Follow Up Required Corrective Action  Supervisor Name Supervisor Email Supervisor Phone Supervisor Office Phone Comp. Man Name Comp. Man Email Comp. Man Phone Comp. Man Office Phone NNE Name NNE Email NNE Phone NNE Office Phone NNE Name NNE Email NNE Phone NNE Office Phone NNE HSE Name NNE HSE Email NNE HSE Number NNE HSE Office Phone SUBMITTEE