Time | State | Township/City | Pad | Latitude | Longitude | 911 Address | Weather | Well Lease | Well # | Well Field | Personnel/Witness Name | Personnel/Wittness Phone | Company | Position | Hitch Days | Years Oil/Gas | Years w/Comp. | Task | Summary | Spill Amount | On containment | Spill contained | NNE Contacted | DEP Contacted | Spill Line Contacted | Notification Timeline | Spill Cleaned Up | Follow Up Required | Corrective Action | Supervisor Name | Supervisor Email | Supervisor Phone | Supervisor Office Phone | Comp. Man Name | Comp. Man Email | Comp. Man Phone | Comp. Man Office Phone | NNE Name | NNE Email | NNE Phone | NNE Office Phone | NNE Name | NNE Email | NNE Phone | NNE Office Phone | NNE HSE Name | NNE HSE Email | NNE HSE Number | NNE HSE Office Phone | SUBMITTEE | |
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02:00 PM | WV | Produced water hauling | Blacksville | Daybrook Development arrived at the Coastal AST site to offload production water into the Coastal AST. The driver hooked up to the ground manifold and started to pressurize the line, at which point the hose between the truck and the ground manifold failed, specifically at the cam lock connection. Approximately 1 BBL of produced water was sprayed onto the ground, outside secondary containment, but remained on pad. The driver immediately shut the truck off and removed all standing water with the truck. Calls were made to supervisors, as well as the District WV DEP Inspector. NNE's first response environmental clean-up vendor was contacted and dispatched for remediation services. DEP Inspector agreed with NNE's reactionary measures and said there was no need to call WV Spill Hotline. | 5 to 100 gallons | Andy Travis | |||||||||||||||||||||||||||||||||||||||||||||
04:00 PM | WV | Dunkard Creek to Kassay Freshwater Transfer Operations | Blacksville | At approximately 12:00 PM, while crews were transferring freshwater to Dyna Tank #1, the pressure gauge on the booster pump at the Matteo site failed. As a result, approximately 1 gallon of freshwater was released onto the ground, but within the pump's containment. The Rock Water employee manning the pump immediately shut down and notified NNE's Water Consultant. Upon investigation, it was discovered the housing for the stem of the gauge failed, not the gauge itself. Crews replaced same and resumed transferring water. | Less than 1 gallon | Andy Travis | |||||||||||||||||||||||||||||||||||||||||||||
02:15 PM | WV | Coastal Tank Farm | Blacksville | At 10:15 AM, April 3, 2017, NNE found a failure in the tank containment on the Coastal Pad. The failure was a six inch cut in the containment, which allowed standing rain water to exit onto the pad - all water released remained on the pad. Notifications were made, the water was tested and results were within the allowable parameters, a sand bag was placed on top of the cut to reduce any additional water from escaping, and crews were dispatched. Daybrook Development was called to remove all remaining water from containment, and RW Products was called to patch the failed portion of the containment. NNE's WV DEP Inspector was called to provide a summary of the incident, and no further direction was given. | Less than 1 gallon | Andy Travis | |||||||||||||||||||||||||||||||||||||||||||||
04:00 PM | WV | Beach Tank Farm | Blacksville | At 12:00 PM, April 3, 2017, NNE found a failure in the tank containment on the Beach Pad. The failure was a six inch cut in the containment, which allowed standing rain water to exit onto the pad - all water released remained on the pad. Notifications were made, the water was tested and results were within the allowable parameters, a sand bag was placed on top of the cut to reduce any additional water from escaping, and crews were dispatched. Daybrook Development was called to remove all remaining water from containment, and RW Products was called to patch the failed portion of the containment. | Less than 1 gallon | Andy Travis | |||||||||||||||||||||||||||||||||||||||||||||
07:15 PM | WV | Kassay | Blacksville | Per Site Supervisor Glenn Boyd: | 5 to 100 gallons | Andy Travis | |||||||||||||||||||||||||||||||||||||||||||||
05:30 PM | WV | Blacksville | 1-1.5 gallon diesel spill on Statler lease road. Rockwater was moving a fuel cell in place for water transfer from the Statler impoundments. The fuel cell was mostly empty. During transport on the forklift a pump broke off allowing the remaining fuel to spill | 1 to 5 gallons | Andy Travis | ||||||||||||||||||||||||||||||||||||||||||||||
06:45 PM | WV | Fisher | Blacksville | During Line inspections today of the Temp Line Running from Coastal to Fisher location. I found a Diesel Spill coming from a Staged BJ Pump Truck. The Fuel has stoped leaking as of now, the Frac Consultant along with BJ was passed the information. | 5 to 100 gallons | Andy Travis | |||||||||||||||||||||||||||||||||||||||||||||
05:10 PM | WV | Fisher | Blacksville | Have a very small Diesel Spill on the Statler Lease Road. The only Party that looks to be at Fault is Jacobs Fuel. Currently Rock Water is Ordering Clean Up services. | 1 to 5 gallons | Andy Travis | |||||||||||||||||||||||||||||||||||||||||||||
03:45 PM | WV | Water Transfer/ Disposal | Blacksville | I just received word from the field that one of the water truck drivers from Ransom Drilling was killed as a result of his truck wrecking. I?m told as he was traveling on Rt. 50 to/from one the disposal facilities in Ohio, the truck blew a tire and he lost control. DOT is on scene and will conduct an investigation. There is a story already on WBOY?s website with two pictures, as well as WDTV?s website. | 80 bbls | Andy Travis | |||||||||||||||||||||||||||||||||||||||||||||
03:23 PM | WV | Water Transfer/ Disposal | Blacksville | While performing our bore at the Jakes Run Stream Crossing we have seeped into the stream bed with our drilling mud. The mud finds a way to the surface from the bore. Bentonite is the only foreign substance in the mud. The stream is milky in color. I notified WVDEP inspector. Inspector Arrived on site at 2:10pm | 1 to 5 gallons | Andy Travis | |||||||||||||||||||||||||||||||||||||||||||||
07:00 PM | WV | Temporary, aboveground waterline between Coastal and Fisher Pads | Blacksville | On 11/21/17 at approximately 4:15 PM and on 11/22/17 at approximately 2:00 PM, as crews were pressure testing the temporary, aboveground waterline between Coastal and Fisher, stress fractures were discovered during the line walks. These fractures allowed freshwater to be released onto the ground. Testing was immediately halted, the line was evacuated, and repairs were made and have been scheduled. The pipe that was delivered for this installation was used previously for other transfer jobs. QAQC was performed on the pipe prior to installation, but due to the nature of these impairments, they could not have been detected until pressure was applied to the line. | 1 to 5 gallons | Andy Travis | |||||||||||||||||||||||||||||||||||||||||||||
08:15 PM | WV | Auxiliary Pad above the Fisher Well Pad | Blacksville | On November 30, 2017 at approximately 3:15 PM, NNE employee arrived onsite at the auxiliary pad above the Fisher Pad and found hydraulic fluid released on the ground where a fusing machine had been sitting. The fusing machine was removed from site, absorbent pads were placed on the contaminated area, and a crew removed the contaminated stone and replaced with clean stone. WV DEP Inspector, Gayne Knitowski, was notified and provided no other action to take. | 1 to 5 gallons | Andy Travis | |||||||||||||||||||||||||||||||||||||||||||||
12:30 PM | WV | Fisher | Blacksville | At 7:30 this morning a 16" temporary above ground waterline owned and operated by Rockwater, parted at a weld during frac operations on the Fisher Pad. The waterline operator had been pumping at 70 bbls/min for a couple of minutes when he noticed a drop in pressure and increase in flow rate. He immediately shut down operations to determine where the potential issue was. The break in the line was found above the Coastal Pad, along the access road that runs between the Fisher and Coastal Pads. We are estimating that 450 bbls of a 30% concentration mixture of produced and fresh water escaped and ran down the hillside and lease road. There are no streams or waterways that connect with the contaminated area. DEP inspector Gayne Knitowski was notifed at 9:00 am this morning, and visited the location. He was supportive of the actions we had taken and asked to be kept in the loop with the NGE plan of action for remediation. DEP spill hotline was contacted at 10:30 am and assigned the following reference number 31-67939. NGE has been brought in to address environmental remediation, and we are scheduling a meeting with Rockwater to address this incident. | 100 gallons or greater | Andy Travis | |||||||||||||||||||||||||||||||||||||||||||||
04:00 PM | WV | Coastal-Campbell Access Road | Blacksville | On 12/13/17 at approximately 11:00 AM, water transfer crew members were relocating a pump from the Campbell Pad to the Dunkard Creek Withdrawal Site and upon transporting the pump, diesel fuel leaked out of the pump's fuel cell in two places along the Coastal-Campbell Access Road. Oil soak rags were immediately placed on the spill areas. The pump was taken to a level area in order to run the pump and use the extra fuel prior to transporting further on uneven terrain and potentially causing further leaking. NNE's HSE Rep and Water Rep talked with crew members about fueling with consideration of transporting pumps. | Environmental > Spill > Petroleum Fuel > 5 to 100 gallons | Andy Travis | |||||||||||||||||||||||||||||||||||||||||||||
06:30 PM | WV | Coastal AST | Blacksville | On 12/13/17 at approximately 1:30 PM, NNE's drilling consultant observed water leaking at a flange on the discharge pipe at the AST. An estimated 2 BBL of blended water was released onto the ground, outside of containment. The water never left the well pad and did not impact any streams. NNE's HSE rep and Water rep went to site to assess situation and put containment under the leak to prevent further spreading. Water transfer crew members were immediately called to break down the flange and identify the failure. Upon breaking the flange down, it was determined the failure was a broken bolt that holds the flange together. Crew members replaced the damaged bolt with a new one, bolted the flange back up, which resolved the issue. | 5 to 100 gallons | Andy Travis | |||||||||||||||||||||||||||||||||||||||||||||
04:30 PM | WV | 39.625547 | -79.963157 | Harvey 1 Well | Blacksville | Crude Oil Soil Contamination at the Harvey 1 Well Initial contact made by DEP Inspector, Gayne Knitowski, on March 2nd regarding oil contaminated soil in the immediate area around the wellhead. Also mentioned oil and grease on the wellhead and stuffing box. This was pre-existing condition of the well prior to acquisition by Northeast. Jeremiah Wilt cleaned wellhead and immediate soil area around the wellhead on March 6th. Gayne was notified via email that day with accompanied pictures of site. Gayne re-visited location on March 21st and raised concerns about remaining contaminated soil as well as berm condition of old tanks. He asked that more remediation efforts be done on contaminated soil and repair of tank berm to avoid threat of violation. NGE Environmental onsite morning of the 22nd to obtain samples/pictures of contaminated soil and develop a plan to remediate areas of concern. Plan to pursue tilling of contaminated soil, liming, and re-seed in accordance with regulations. | 5 to 100 gallons | Andy Travis | |||||||||||||||||||||||||||||||||||||||||||
01:00 PM | WV | Grant Dist., Monongalia Co. | N/A | 39.615723 | -80.089051 | N/A | Overcast | Michael | Mon River Waterline | Blacksville | Anthony Carlson | (304) 216-8886 | Solo Construction | Water Consultant | 7 | 10 | 8 | Following up on notification that a diesel spill had occurred at the Booster #2 pump station on the Mon River Waterline. | On 03 Jan 19, at approximately 1:00 PM, a diesel spill was discovered at Booster #2 pump station on the Mon River Waterline, outside secondary containment and estimated to be 5 gallons. No waters of the state or US were affected. It was determined this occurred near the end of the last transfer activity and went unreported. After discovery, a crew was dispatched to remove the contaminated stone and replace with new stone. The Spill Hotline was called and provided the following reference number: 31-84925. DEP Waste and Water Inspector Travis Hayes is also aware of the spill and the remedial actions taken. | 5 gallons | No | Yes | Yes | Yes | Yes | 01/03/19, 1 PM - Spill Discovery & DEP notification; 4:30 PM - Spill Hotline | Yes | Yes | Removed contaminated stone and replaced with new stone | Casey Buckhanan | Email hidden; Javascript is required. | (304) 224-5567 | (304) 224-5567 | Anthony Carlson | Email hidden; Javascript is required. | (304) 216-8886 | (304) 216-8886 | Chris Patterson | Email hidden; Javascript is required. | (304) 203-7034 | (304) 212-0417 | Hollie Medley | Email hidden; Javascript is required. | (304) 543-8932 | (304) 212-0422 | Andy Travis | Email hidden; Javascript is required. | (304) 951-0909 | (304) 212-0415 | Chris Patterson | |
09:00 AM | WV | Maidsville | Boggess | 39.671520 | -80.089826 | 2030 Mason Dixon Hwy, Maidsville, WV 26541 | Sunny | Boggess | 5H | Blacksville | Jay Hewitt | (304) 382-1825 | Hewitt Energy Strategies | Owner | 4 | 15 | 1 | During an inspection of the backyard area, stressed vegetation was noticed on the backside of the Boggess pad. It appeared and was later confirmed that the source of the spill was base oil/drilling mud. | A flow line connecting the mud pits had a slow leak and had been dripping for some time. The location of the line is not readily visible without climbing between the tanks. The entire backyard area is on containment and matted. Unfortunately the leak accumulated over time and found its way under the containment due to a small hole under the matting. I contacted WVDEP, Gayne asked that we get the spill contained to make sure that it does not leave our LOD, and gave us permission for now to continue with drilling operations. Clean up will be done once the rig is moved off of location. | Estimate of 2 bbl spill | Spill is outside of containment | Spill has been contained | NNE contacted 5/23/2019 at 9:00 | Gayne Knitowski was contacted | Not at this time | Immediate Notification | Spill has not been cleaned up | Spill can be cleaned once rig leaves | Better housekeeping around mud pits | Jay Hewitt | Email hidden; Javascript is required. | (304) 382-1825 | (304) 382-1825 | Troy Hamidi | Email hidden; Javascript is required. | (719) 459-2067 | (719) 459-2067 | Josh Dalton | Email hidden; Javascript is required. | (304) 212-0424 | (304) 212-0424 | Hollie Medley | Email hidden; Javascript is required. | (304) 543-8932 | (304) 212-0422 | Andy Travis | Email hidden; Javascript is required. | (304) 951-0909 | (304) 212-0415 | Andy Travis | |
06:30 AM | WV | Fairview | McClellan | 39.667166 | -80.096846 | 326 Harvey Run Road, Fairview wv | Cool & Rainy | McClellan | 6H | Battelle | Bobby Gilbert | (903) 486-2689 | Patterson | Toolpusher | 9 | 15 | 15 | Pumping slug to finish tripping out of hole | While tripping out of the hole, the fluid flow path was connected to the trip tank as normal. When it was time to pump a slug, the Driller called on radio for derrick hand to line up on the flow line and off the trip tank. The derrick hand confirmed the flowline was ready. Driller began pumping and immediately noticed an increase in pump pressure and shut off pumps. The back yard came across radio and said he was seeing mud coming across the choke skid. After investigation the main flowline valve was left closed causing pressure to build up and blow out the seal between the flowline and elkhorn. There was a miss communication, and the motorman shut the valve while the derrick hand was in the derrick tripping pipe. The derrick hand assumed the valve was still open. | 16 barrels | All except 10 gallons | All except 10 gallons | Yes, Sam Barker, Josh Dalton & Andy Travis | Yes, Bryan Harris inspector | No | Immediately to NNE. Couple hrs later for inspector to return call. | Outside of containment has been cleaned up, waiting on clean up crew to clean rig and mats | After rig is moved off we will clean up mats and plastic under mats | Shut down, have safety meeting, clean up gravel outside of containment, re connect flowline to elkhorn, chain down hammer seal | Bobby Gilbert | Email hidden; Javascript is required. | (903) 486-2689 | (903) 486-2689 | Sam Barker | Email hidden; Javascript is required. | (304) 629-2284 | (304) 629-2284 | Josh Dalton | Email hidden; Javascript is required. | (724) 825-6859 | (724) 825-6859 | Hollie Medley | Email hidden; Javascript is required. | (304) 543-8932 | (304) 212-0422 | Andy Travis | Email hidden; Javascript is required. | (304) 951-0909 | (304) 212-0415 | Josh Dalton | |
11:30 AM | WV | Maidsville | Jenkins | 39.711342° | -80.139292° | 3835 Mason Dixon Hwy, Maidsville WV 26541 | Sunny | Jenkins | Rig Move | Blacksville | Josh Frazier | (304) 517-6188 | NE Safety Solutions | Safety Consultant | 2 | 10 | 1 | While performing a site inspection, Josh Frazier noticed that there was a track of fluid spilled onto the Jenkins location road staging area. | After the rig move, Josh Frazier pulled onto location to perform a safety check and noticed a track of fluid where we had staged some of the Patterson equipment for the move, He notified supervision which in turn notified NNE Compnayman Josh Grim. Josh went out to check the area and get Chisler Brothers out to perform the clean up. By the time I had reached the location Chisler was already there and had absorbant on the spill and were prepping to scrape up any contamination and haul it off to be disposed of. | Less than one gallon | Spill was off containment on gravel staging area | The spill area was limited to the staging area | Josh Frazier notified as soon as spill was discovered | DEP inspector Gayne Knitowski was notified by voicemail | Spill line has not been contacted | Notification came from random safety inspection | Spill cleaned up | No follow up required | Need to do site inspection after move | Josh Grim | Email hidden; Javascript is required. | (304) 276-3899 | (304) 276-3899 | Josh Grim | Email hidden; Javascript is required. | (304) 276-3899 | (304) 276-3899 | Jay Hewitt | Email hidden; Javascript is required. | (304) 382-1825 | (304) 382-1825 | Hollie Medley | Email hidden; Javascript is required. | (304) 543-8932 | (304) 212-0422 | Andy Travis | Email hidden; Javascript is required. | (304) 951-0909 | (304) 212-0415 | Andy Travis | |
08:35 PM | WV | Fairview | Lemley Frac | 39.662820 | -80.166166 | Mount Harmon Rd | Clear | Lemley | n/a | Blacksville | Emily Stier | (304) 709-1980 | NSJ for Bear Contracting | Water Line Inspection | 4 | 6 | 2 | Water line ARV inspection | While inspecting the Kassay MEPCO line on night shift, a spill was observed coming from the ARV located on the Eddie Sine property. The ARV was locked and other than the water leaking out of the vault appeared to be in good condition. Attempts were made to close the valve to shut off the flow of additional water. Anthony Carlson was notified and drove out to location from his home, he was able reach into the vault while full of produced water and shut the valve below the ARV assembly, which stopped the flow of additional water at approximately 10:30 pm Friday night. | Unknown quantity | Spill was out of containment | Spill was not contained but was stopped | NNE was contacted immediately | Contacted Bryan Harris Saturday 6/26/2021 | Called in to spill hotline 9am on 6/26/2021 ref # 31-15727 | Immediate Notification | Spill has not been cleaned up | Follow up required | Corrective action TBD | Rob Feathers | Email hidden; Javascript is required. | (304) 918-8993 | (304) 918-8993 | Anthony Carlson | Email hidden; Javascript is required. | (304) 216-8886 | (304) 216-8886 | Chris Patterson | Email hidden; Javascript is required. | (304) 203-7034 | (304) 212-0417 | Hollie Medley | Email hidden; Javascript is required. | (304) 543-8932 | (304) 212-0422 | Andy Travis | Email hidden; Javascript is required. | (304) 951-0909 | (304) 212-0415 | Andy Travis | |
06:25 PM | WV | Clay | Mepco | 39.662737 | -80.166485 | 579 Mepco Road, Fairview, WV 26570 | Rainy | Mepco | 2H & 4H | Blacksville | Jeff Wilson | (304) 480-1414 | Solo Construction | Water Consultant | 5 | 25 | 8 | No active task at time of notification of release. | On 9/16/18, at approximately 6:25 PM, NNE was notified by a landowner that water was overflowing an air release valve (ARV) vault and running down the hill. Landowner also notified WV DEP of the incident. NNE made notifications to supervision and dispatched field personnel to visually inspect the site and ensure the leaking had stopped. Once field personnel arrived at ARV site, water was still leaking and detected a one-inch drain valve was open on the bottom of the ARV. The valve was shut and the leaking stopped. Environmental contractor was called to bring erosion controls and gather water and soil samples to begin the remediation process. NNE personnel met with WV DEP Inspector, Gayne Knitowski, to review the site and discuss next steps. Remediation efforts will be ongoing until site is vacant of all contaminated material. Spill hotline was called and NNE was provided reference number 31-80825. | 635 | No | No | Yes | Yes | Yes | 9/16/18, 6:25 PM - Notification of spill; 9/17/18, 10:00 AM - meeting onsite with DEP Inspector; 9/17/18, 3:00 PM - erosion controls installed; 9/18/18, 8:00 AM - water/soil samples gathered | No | Yes | Remediate site until all contaminated materials are removed | Chris Patterson | Email hidden; Javascript is required. | (304) 203-7034 | (304) 212-0417 | Chris Patterson | Email hidden; Javascript is required. | (304) 203-7034 | (304) 212-0417 | Chris Patterson | Email hidden; Javascript is required. | (304) 203-7034 | (304) 212-0417 | Hollie Medley | Email hidden; Javascript is required. | (304) 543-8932 | (304) 212-0422 | Andy Travis | Email hidden; Javascript is required. | (304) 951-0909 | (304) 212-0415 | Chris Patterson | |
09:35 PM | WV | Coastal | 39.705903 | -80.203933 | 1001 Daybrook Rd, Fairview WV 26570 | Blacksville | When transporting SBM tank from Fisher to Coastal the truck started down hill and about 1 bbl of SBM splashed out of vent cap on top of tank. It then began to drip down on the lease road. It remained contained to the lease road. | 5 to 100 gallons | Andy Travis | ||||||||||||||||||||||||||||||||||||||||||
02:00 PM | WV | Coastal | 39.705903 | -80.203933 | 1001 Daybrook Rd, Fairview WV 26570 | Blacksville | While delivering a load of fuel to location, diesel was spotted underneath the fuel truck every time he came to a stop. We followed the truck and immediately got him up on containment and placed a drip pan under the leak. Once the leak was contained we began immediate transfer of fuel from the truck to the diesel tank so we could empty out the fuel load. The drivers name was Rick Bowser (330-847-0087) driving truck #25, He is employed by Mike Ainsley (330-727-1414) of Ainsley oil and has 3 Yrs with the company, 15 years driving experience. | Less than 1 gallon | Andy Travis | ||||||||||||||||||||||||||||||||||||||||||
10:30 AM | WV | Fairview | Coastal | 39.705903 | -80.203933 | 1001 Daybrook Rd, Fairview WV 26570 | Sunny | Coastal | 6H | Blacksville | Max Oliver | (817) 526-4147 | ARC | Frac Consultant | 45 | 38 | 7 | As we finished Coastal 6H stg 13, one of the hands called on the radio to tell us there was an FR spill. Went back and checked, a load of FR was delivered during the stage, the driver was told not to blow off until we were finished. (it causes the FR pumps to lose prime). Evidently, he left the pump running and left. I don’t know where he went. When the Producers guys found it there was a large quantity of FR on the containment, pumps, pump room and a small amount beside the containment. There is even a thin film on the side of the AST. | Driver – Richard Charles says he owns Charco Three the trucking company. Truck Tag AG 68768 Pennsylvania Trailer Tag PT 672E2, Copy of CDL attached, did not have any proof of insurance When asked why he was pumping after being told not to pump, he claimed no one told him. I believe this statement to be an absolute untruth. I asked him his name, I asked his employer and he told me Flowtek, I asked for his supervisors number and he gave me Rick Shaner 412-452-4032. I called Rick and found out Richard doesn’t work for Flowtek. I doubt almost everything the guy has told me. The estimated volume at this time is 100 gallons until we know better. (really hard to tell how much some is on top of pumps. We have captured as much as we can off of containment, cut the saturated felt up. The small amount off containment has been soaked with moss and will be picked up and contained. The containment is being cut out and repaired were it is soaked. Hopefully, we will be back in operation within the next hour or two, as soon as the mat is repaired and the trucks re-spotted. | 300 Gallons | 298 Gallons | Spill was contained | Contacted Criss VanGuilder | Gayne Knitowski | Not Req | 2 hrs | Spill Cleaned (6 hours) | None | Pending | Shane Stephenson | Email hidden; Javascript is required. | (740) 586-8729 | (740) 454-6253 | Max Oliver | Email hidden; Javascript is required. | (817) 526-4147 | (817) 526-4147 | Criss VanGuilder | Email hidden; Javascript is required. | (405) 757-8725 | (304) 212-0423 | Hollie Medley | Email hidden; Javascript is required. | (304) 543-8932 | (304) 212-0422 | Andy Travis | Email hidden; Javascript is required. | (304) 951-0909 | (304) 212-0415 | Andy Travis | |
Time | State | Township/City | Pad | Latitude | Longitude | 911 Address | Weather | Well Lease | Well # | Well Field | Personnel/Witness Name | Personnel/Wittness Phone | Company | Position | Hitch Days | Years Oil/Gas | Years w/Comp. | Task | Summary | Spill Amount | On containment | Spill contained | NNE Contacted | DEP Contacted | Spill Line Contacted | Notification Timeline | Spill Cleaned Up | Follow Up Required | Corrective Action | Supervisor Name | Supervisor Email | Supervisor Phone | Supervisor Office Phone | Comp. Man Name | Comp. Man Email | Comp. Man Phone | Comp. Man Office Phone | NNE Name | NNE Email | NNE Phone | NNE Office Phone | NNE Name | NNE Email | NNE Phone | NNE Office Phone | NNE HSE Name | NNE HSE Email | NNE HSE Number | NNE HSE Office Phone | SUBMITTEE |