Time | State | Township/City | Pad | Latitude | Longitude | 911 Address | Weather | Well Lease | Well # | Well Field | Personnel/Witness Name | Personnel/Wittness Phone | Company | Position | Hitch Days | Years Oil/Gas | Years w/Comp. | Task | Summary | Spill Amount | On containment | Spill contained | NNE Contacted | DEP Contacted | Spill Line Contacted | Notification Timeline | Spill Cleaned Up | Follow Up Required | Corrective Action | Supervisor Name | Supervisor Email | Supervisor Phone | Supervisor Office Phone | Comp. Man Name | Comp. Man Email | Comp. Man Phone | Comp. Man Office Phone | NNE Name | NNE Email | NNE Phone | NNE Office Phone | NNE Name | NNE Email | NNE Phone | NNE Office Phone | NNE HSE Name | NNE HSE Email | NNE HSE Number | NNE HSE Office Phone | SUBMITTEE | |
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04:00 PM | WV | Dunkard Creek to Kassay Freshwater Transfer Operations | Blacksville | At approximately 12:00 PM, while crews were transferring freshwater to Dyna Tank #1, the pressure gauge on the booster pump at the Matteo site failed. As a result, approximately 1 gallon of freshwater was released onto the ground, but within the pump's containment. The Rock Water employee manning the pump immediately shut down and notified NNE's Water Consultant. Upon investigation, it was discovered the housing for the stem of the gauge failed, not the gauge itself. Crews replaced same and resumed transferring water. | Less than 1 gallon | Andy Travis | |||||||||||||||||||||||||||||||||||||||||||||
07:00 PM | WV | Temporary, aboveground waterline between Coastal and Fisher Pads | Blacksville | On 11/21/17 at approximately 4:15 PM and on 11/22/17 at approximately 2:00 PM, as crews were pressure testing the temporary, aboveground waterline between Coastal and Fisher, stress fractures were discovered during the line walks. These fractures allowed freshwater to be released onto the ground. Testing was immediately halted, the line was evacuated, and repairs were made and have been scheduled. The pipe that was delivered for this installation was used previously for other transfer jobs. QAQC was performed on the pipe prior to installation, but due to the nature of these impairments, they could not have been detected until pressure was applied to the line. | 1 to 5 gallons | Andy Travis | |||||||||||||||||||||||||||||||||||||||||||||
05:30 PM | WV | Blacksville | 1-1.5 gallon diesel spill on Statler lease road. Rockwater was moving a fuel cell in place for water transfer from the Statler impoundments. The fuel cell was mostly empty. During transport on the forklift a pump broke off allowing the remaining fuel to spill | 1 to 5 gallons | Andy Travis | ||||||||||||||||||||||||||||||||||||||||||||||
06:30 PM | WV | Coastal AST | Blacksville | On 12/13/17 at approximately 1:30 PM, NNE's drilling consultant observed water leaking at a flange on the discharge pipe at the AST. An estimated 2 BBL of blended water was released onto the ground, outside of containment. The water never left the well pad and did not impact any streams. NNE's HSE rep and Water rep went to site to assess situation and put containment under the leak to prevent further spreading. Water transfer crew members were immediately called to break down the flange and identify the failure. Upon breaking the flange down, it was determined the failure was a broken bolt that holds the flange together. Crew members replaced the damaged bolt with a new one, bolted the flange back up, which resolved the issue. | 5 to 100 gallons | Andy Travis | |||||||||||||||||||||||||||||||||||||||||||||
09:35 PM | WV | Coastal | 39.705903 | -80.203933 | 1001 Daybrook Rd, Fairview WV 26570 | Blacksville | When transporting SBM tank from Fisher to Coastal the truck started down hill and about 1 bbl of SBM splashed out of vent cap on top of tank. It then began to drip down on the lease road. It remained contained to the lease road. | 5 to 100 gallons | Andy Travis | ||||||||||||||||||||||||||||||||||||||||||
02:15 PM | WV | Coastal Tank Farm | Blacksville | At 10:15 AM, April 3, 2017, NNE found a failure in the tank containment on the Coastal Pad. The failure was a six inch cut in the containment, which allowed standing rain water to exit onto the pad - all water released remained on the pad. Notifications were made, the water was tested and results were within the allowable parameters, a sand bag was placed on top of the cut to reduce any additional water from escaping, and crews were dispatched. Daybrook Development was called to remove all remaining water from containment, and RW Products was called to patch the failed portion of the containment. NNE's WV DEP Inspector was called to provide a summary of the incident, and no further direction was given. | Less than 1 gallon | Andy Travis | |||||||||||||||||||||||||||||||||||||||||||||
08:15 PM | WV | Auxiliary Pad above the Fisher Well Pad | Blacksville | On November 30, 2017 at approximately 3:15 PM, NNE employee arrived onsite at the auxiliary pad above the Fisher Pad and found hydraulic fluid released on the ground where a fusing machine had been sitting. The fusing machine was removed from site, absorbent pads were placed on the contaminated area, and a crew removed the contaminated stone and replaced with clean stone. WV DEP Inspector, Gayne Knitowski, was notified and provided no other action to take. | 1 to 5 gallons | Andy Travis | |||||||||||||||||||||||||||||||||||||||||||||
06:45 PM | WV | Fisher | Blacksville | During Line inspections today of the Temp Line Running from Coastal to Fisher location. I found a Diesel Spill coming from a Staged BJ Pump Truck. The Fuel has stoped leaking as of now, the Frac Consultant along with BJ was passed the information. | 5 to 100 gallons | Andy Travis | |||||||||||||||||||||||||||||||||||||||||||||
04:30 PM | WV | 39.625547 | -79.963157 | Harvey 1 Well | Blacksville | Crude Oil Soil Contamination at the Harvey 1 Well Initial contact made by DEP Inspector, Gayne Knitowski, on March 2nd regarding oil contaminated soil in the immediate area around the wellhead. Also mentioned oil and grease on the wellhead and stuffing box. This was pre-existing condition of the well prior to acquisition by Northeast. Jeremiah Wilt cleaned wellhead and immediate soil area around the wellhead on March 6th. Gayne was notified via email that day with accompanied pictures of site. Gayne re-visited location on March 21st and raised concerns about remaining contaminated soil as well as berm condition of old tanks. He asked that more remediation efforts be done on contaminated soil and repair of tank berm to avoid threat of violation. NGE Environmental onsite morning of the 22nd to obtain samples/pictures of contaminated soil and develop a plan to remediate areas of concern. Plan to pursue tilling of contaminated soil, liming, and re-seed in accordance with regulations. | 5 to 100 gallons | Andy Travis | |||||||||||||||||||||||||||||||||||||||||||
03:23 PM | WV | Water Transfer/ Disposal | Blacksville | While performing our bore at the Jakes Run Stream Crossing we have seeped into the stream bed with our drilling mud. The mud finds a way to the surface from the bore. Bentonite is the only foreign substance in the mud. The stream is milky in color. I notified WVDEP inspector. Inspector Arrived on site at 2:10pm | 1 to 5 gallons | Andy Travis | |||||||||||||||||||||||||||||||||||||||||||||
04:00 PM | WV | Beach Tank Farm | Blacksville | At 12:00 PM, April 3, 2017, NNE found a failure in the tank containment on the Beach Pad. The failure was a six inch cut in the containment, which allowed standing rain water to exit onto the pad - all water released remained on the pad. Notifications were made, the water was tested and results were within the allowable parameters, a sand bag was placed on top of the cut to reduce any additional water from escaping, and crews were dispatched. Daybrook Development was called to remove all remaining water from containment, and RW Products was called to patch the failed portion of the containment. | Less than 1 gallon | Andy Travis | |||||||||||||||||||||||||||||||||||||||||||||
12:30 PM | WV | Fisher | Blacksville | At 7:30 this morning a 16" temporary above ground waterline owned and operated by Rockwater, parted at a weld during frac operations on the Fisher Pad. The waterline operator had been pumping at 70 bbls/min for a couple of minutes when he noticed a drop in pressure and increase in flow rate. He immediately shut down operations to determine where the potential issue was. The break in the line was found above the Coastal Pad, along the access road that runs between the Fisher and Coastal Pads. We are estimating that 450 bbls of a 30% concentration mixture of produced and fresh water escaped and ran down the hillside and lease road. There are no streams or waterways that connect with the contaminated area. DEP inspector Gayne Knitowski was notifed at 9:00 am this morning, and visited the location. He was supportive of the actions we had taken and asked to be kept in the loop with the NGE plan of action for remediation. DEP spill hotline was contacted at 10:30 am and assigned the following reference number 31-67939. NGE has been brought in to address environmental remediation, and we are scheduling a meeting with Rockwater to address this incident. | 100 gallons or greater | Andy Travis | |||||||||||||||||||||||||||||||||||||||||||||
05:10 PM | WV | Fisher | Blacksville | Have a very small Diesel Spill on the Statler Lease Road. The only Party that looks to be at Fault is Jacobs Fuel. Currently Rock Water is Ordering Clean Up services. | 1 to 5 gallons | Andy Travis | |||||||||||||||||||||||||||||||||||||||||||||
02:00 PM | WV | Produced water hauling | Blacksville | Daybrook Development arrived at the Coastal AST site to offload production water into the Coastal AST. The driver hooked up to the ground manifold and started to pressurize the line, at which point the hose between the truck and the ground manifold failed, specifically at the cam lock connection. Approximately 1 BBL of produced water was sprayed onto the ground, outside secondary containment, but remained on pad. The driver immediately shut the truck off and removed all standing water with the truck. Calls were made to supervisors, as well as the District WV DEP Inspector. NNE's first response environmental clean-up vendor was contacted and dispatched for remediation services. DEP Inspector agreed with NNE's reactionary measures and said there was no need to call WV Spill Hotline. | 5 to 100 gallons | Andy Travis | |||||||||||||||||||||||||||||||||||||||||||||
02:00 PM | WV | Coastal | 39.705903 | -80.203933 | 1001 Daybrook Rd, Fairview WV 26570 | Blacksville | While delivering a load of fuel to location, diesel was spotted underneath the fuel truck every time he came to a stop. We followed the truck and immediately got him up on containment and placed a drip pan under the leak. Once the leak was contained we began immediate transfer of fuel from the truck to the diesel tank so we could empty out the fuel load. The drivers name was Rick Bowser (330-847-0087) driving truck #25, He is employed by Mike Ainsley (330-727-1414) of Ainsley oil and has 3 Yrs with the company, 15 years driving experience. | Less than 1 gallon | Andy Travis | ||||||||||||||||||||||||||||||||||||||||||
07:15 PM | WV | Kassay | Blacksville | Per Site Supervisor Glenn Boyd: | 5 to 100 gallons | Andy Travis | |||||||||||||||||||||||||||||||||||||||||||||
04:00 PM | WV | Coastal-Campbell Access Road | Blacksville | On 12/13/17 at approximately 11:00 AM, water transfer crew members were relocating a pump from the Campbell Pad to the Dunkard Creek Withdrawal Site and upon transporting the pump, diesel fuel leaked out of the pump's fuel cell in two places along the Coastal-Campbell Access Road. Oil soak rags were immediately placed on the spill areas. The pump was taken to a level area in order to run the pump and use the extra fuel prior to transporting further on uneven terrain and potentially causing further leaking. NNE's HSE Rep and Water Rep talked with crew members about fueling with consideration of transporting pumps. | Environmental > Spill > Petroleum Fuel > 5 to 100 gallons | Andy Travis | |||||||||||||||||||||||||||||||||||||||||||||
03:45 PM | WV | Water Transfer/ Disposal | Blacksville | I just received word from the field that one of the water truck drivers from Ransom Drilling was killed as a result of his truck wrecking. I?m told as he was traveling on Rt. 50 to/from one the disposal facilities in Ohio, the truck blew a tire and he lost control. DOT is on scene and will conduct an investigation. There is a story already on WBOY?s website with two pictures, as well as WDTV?s website. | 80 bbls | Andy Travis | |||||||||||||||||||||||||||||||||||||||||||||
05:30 PM | WV | Fairview | Paw Paw Intake | 39.5875343477431 | -80.2380556338929 | 39.587534,-80.238055 | Sunny | n/a | n/a | Paw Paw | Clint George | (330) 464-6401 | East Coast Underground (Sub To Ready Field Solutions) | Supervisor | 1 | Reclamation of Paw Paw Creek road bore | While reclaiming the Paw Paw Creek road bore, the operator struck an unmarked 3" water line . Fairview water department was notified and shut the water off after approximately 1 hour. There was enough water that the super silt fence and silt sock were compromised and allowed fresh water to flow into Paw Paw Creek. | Unknown | out of contaiment | Spill has been contained | NNE contacted 6:00 3/9/2020 | Reported spill to Travis Hays 6:28pm 3/9/2020 | Spill hot line reported 3/10/2020 @ 8:45am ref # 25-100308 | Immediate | unknown | Follow up meeting scheduled for 3/11/2020 | unknown | Clint George | Email hidden; Javascript is required. | (330) 464-6401 | (330) 464-6401 | MIke Shreve | Email hidden; Javascript is required. | (304) 918-3050 | (304) 918-3050 | Dave McDougal | Email hidden; Javascript is required. | (304) 212-0419 | (304) 212-0419 | Hollie Medley | Email hidden; Javascript is required. | (304) 543-8932 | (304) 212-0422 | Andy Travis | Email hidden; Javascript is required. | (304) 951-0909 | (304) 212-0415 | Andy Travis | |||
11:10 AM | WV | Fairview | Cummins | 1776892.4 | 423957.93 | 2575 Daybrook Rd. Fairview, WV 26570 | 40º / çloudy | Cummins | 6H | Blacksville | Reggie Neil | (234) 855-5874 | CS Trucking | Driver | 1 | 10 | 7 | Delivering base oil to the Cummins Pad | While delivering base oil to the HZ rig on the Cummins pad, the truck blew a radiator hose traveling inbound to the Matteo/Kassay/Cummins pads. As he reached the hilltop, he saw steam coming from under the hood. The driver continued up the hill to a safe spot to pull over just before the Matteo Pad next to the guard shack. The driver used absorbent pads to clean up the radiator fluid. Company man made several passes up and down the road searching for any additional spillage but was unable to locate any. Company man had driver back up truck, place new absorbent pads underneath, cleaned up all radiator fluid on ground, and the driver waited for mechanic to arrive to do repairs. Less than 1 gallon was visibly on the ground and was immediately cleaned up. | less than 1 gallon | no | no | Yes | No | No | Immediately | Yes | None | None | Pedro Robles | Email hidden; Javascript is required. | (770) 894-3276 | (770) 894-3276 | Troy Hamidi | Email hidden; Javascript is required. | (304) 629-2284 | (304) 629-2284 | Josh Dalton | Email hidden; Javascript is required. | (724) 825-6859 | (724) 825-6859 | Hollie Medley | Email hidden; Javascript is required. | (304) 543-8932 | (304) 212-0422 | Andy Travis | Email hidden; Javascript is required. | (304) 951-0909 | (304) 212-0415 | Josh Dalton | |
02:00 PM | WV | Blacksville | Coastal | 39.705639 | -80.204444 | 1001 Daybrook Road, Fairview, WV 26570 | Sunny | Coastal | AST | Blacksville | Bronson Martin | (702) 904-4301 | Comtech Inudstries, Inc. | Laborer | 1 | 1.5 | 1.5 | Re-fueling a portable heater unit. | "While re-fueling a third piece of equipment (a portable heater unit) the transfer / pump hose split and began to spray / release diesel fuel. The employee immediately shut down the pump and began to place spill pads to absorb the fuel. The fuel was on the bed of the truck as well as on the ground. Before the truck was moved it was cleaned to verify no additional areas would be affected. Approximately 2 - 4 gallons of diesel fuel was released (see attached photos). The spill area was cleaned up by placing the soiled spill pads and any dirt / rocks, that were affected, into collection buckets for disposal. The hose transfer line on the fuel cell was immediately replaced." | 2 - 4 gallons | No | Yes | Yes | No | No | 2:00 PM - spill occurred; 2:43 PM - Comtech notified NNE | Yes | No | Replaced split / failed hose on the transfer pump of the fuel cell; modify inspection procedure of fuel cell to include routine replacement of the transfer hose (at least every 6 months). | Levi Bristor | Email hidden; Javascript is required. | (724) 263-0105 | (724) 263-0105 | Anthony Carlson | Email hidden; Javascript is required. | (304) 216-8886 | (304) 216-8886 | Chris Patterson | Email hidden; Javascript is required. | (304) 203-7034 | (304) 212-0417 | Hollie Medley | Email hidden; Javascript is required. | (304) 543-8932 | (304) 212-0422 | Andy Travis | Email hidden; Javascript is required. | (304) 951-0909 | (304) 212-0415 | Chris Patterson | |
10:30 PM | WV | Daybrook/Monongalia | Matteo | N 421911.5 | E 1771644.9 | 25 Yank Hollow Road Fairview, WV 26570 | Clear | Matteo | 4H | Blacksville | Michael Reed | (337) 344-4939 | NOV Solids | Night shift lead | 1 | 3 | 1.5 | Drilling operations, normal AFRS operations of backyard equipment running trough, pumps, and centrifuge equipment. | During drilling operations the NOV AFRS system failed to alarm the operators of a high fluid level and go into fail safe shutting down the pumps and flipping the "whale tail". This resulted in the trough overfilling and spilling out over the backside out of view releasing ~20Bbl of OBM onto containment. As soon as run over was spotted system was manually shut down by night shift lead(Michael Reed) and cleanup began. | 20Bbl | On Containment | Yes | Josh Dalton/Andy Travis | Andy Travis contacted DEP | unknown | Imediatley | Everything that could be cleaned up was moved and cleaned under matting and above | unknown | Clean up and reconfigure alarm to sequence auto shutdown. | Steven Wojoich | Email hidden; Javascript is required. | (412) 452-1785 | (412) 452-1785 | Joshua Grim | Email hidden; Javascript is required. | (304) 276-3899 | (304) 276-3899 | Josh Dalton | Email hidden; Javascript is required. | (724) 825-6859 | (724) 825-6859 | Hollie Medley | Email hidden; Javascript is required. | (304) 543-8932 | (304) 212-0422 | Andy Travis | Email hidden; Javascript is required. | (304) 951-0909 | (304) 212-0415 | ||
01:00 PM | WV | Fairview | Fisher/Coastal/Campbell access road | 39.694428° | -80.221339° | 1003 Daybrook Rd | Partly Cloudy | Fisher | n/a | Blacksville | Andy Travis | (304) 951-0909 | NNE | HSE Coordinator | 2 | 11 | 4 | While conducting a field review I noticed a spill on the access road. I contacted Chris Patterson to check on any reported water truck spills. The majority of the traffic at this time is water trucks moving water from the Fisher pad, and DTE coopers run facility upgrade. Chris checked with the field coordinators, and received 2 conflicting reports claiming to have witnessed the spill. One report from ECM claimed that a Daybrook water truck leaked the fluid, and the other Report from Ransom claimed that a truck hauling a gooseneck trailer spilled the fluid. The spilled substance had a petroleum odor, but was green in appearance, could have been oil or a mixture. | Mike Shreve called out Chisler Brothers to cleanup contaminated materials , and replace with fresh gravel. Cleanup was completed within 2 hours of finding spill. | 1 gallon or less | Not on containment | Spill was limited to access road | NNE was not notified | Called spill into WVDEP inspector Gayne Knitkowski | Not required to be reported through spill hotline | NNE was not notified of spill | Spill cleaned up (1 hour) | No follow up required for spill | Stress the importance of reporting in safety meetings | Andy Travis | Email hidden; Javascript is required. | (304) 951-0909 | (304) 212-0415 | Andy Travis | Email hidden; Javascript is required. | (304) 951-0909 | (304) 212-0415 | Andy Travis | Email hidden; Javascript is required. | (304) 951-0909 | (304) 212-0415 | Hollie Medley | Email hidden; Javascript is required. | (304) 543-8932 | (304) 212-0422 | Andy Travis | Email hidden; Javascript is required. | (304) 951-0909 | (304) 212-0415 | Andy Travis | |
12:45 PM | WV | Monongalia County | Coastal | 39.705639 | -80.204444 | 1001 Daybrook Road, Fairview, WV 26570 | Overcast | Coastal | Coastal | Blacksville | Josh Null | (304) 599-8384 | RW Products | Manager | 2 | 6 | 6 | Crew was on the Coastal Pad removing solids from the AST, loading into vac boxes, and making ready for transport to disposal. | After the solids removal crew loaded one of the vac boxes, it was relocated from the work area to the staging area to wait for transport to disposal. As it was being unloaded from the roll-off truck to the staging area, the hatch door wasn't fully closed and allowed some of the solids/sludge to escape and spill onto the pad, outside secondary containment. The solids removal crew cleaned up the sludge and dressed in the area with new stone. | 5 gallons | No | Yes | Yes | No | No | 01/07/19, 12:45 PM - Notified of spill | Yes | No | Ensure all doors on vac boxes are shut and fully bound with chain binders; incorporate into JSAs going forward. | Pat Justice | Email hidden; Javascript is required. | (681) 285-5040 | (304) 277-1110 | Jeff Wilson | Email hidden; Javascript is required. | (304) 480-1414 | (304) 480-1414 | Chris Patterson | Email hidden; Javascript is required. | (304) 203-7034 | (304) 212-0417 | Hollie Medley | Email hidden; Javascript is required. | (304) 543-8932 | (304) 212-0422 | Andy Travis | Email hidden; Javascript is required. | (304) 951-0909 | (304) 212-0415 | Chris Patterson | |
11:30 AM | WV | Maidsville | Jenkins | 39.711342° | -80.139292° | 3835 Mason Dixon Hwy, Maidsville WV 26541 | Sunny | Jenkins | Rig Move | Blacksville | Josh Frazier | (304) 517-6188 | NE Safety Solutions | Safety Consultant | 2 | 10 | 1 | While performing a site inspection, Josh Frazier noticed that there was a track of fluid spilled onto the Jenkins location road staging area. | After the rig move, Josh Frazier pulled onto location to perform a safety check and noticed a track of fluid where we had staged some of the Patterson equipment for the move, He notified supervision which in turn notified NNE Compnayman Josh Grim. Josh went out to check the area and get Chisler Brothers out to perform the clean up. By the time I had reached the location Chisler was already there and had absorbant on the spill and were prepping to scrape up any contamination and haul it off to be disposed of. | Less than one gallon | Spill was off containment on gravel staging area | The spill area was limited to the staging area | Josh Frazier notified as soon as spill was discovered | DEP inspector Gayne Knitowski was notified by voicemail | Spill line has not been contacted | Notification came from random safety inspection | Spill cleaned up | No follow up required | Need to do site inspection after move | Josh Grim | Email hidden; Javascript is required. | (304) 276-3899 | (304) 276-3899 | Josh Grim | Email hidden; Javascript is required. | (304) 276-3899 | (304) 276-3899 | Jay Hewitt | Email hidden; Javascript is required. | (304) 382-1825 | (304) 382-1825 | Hollie Medley | Email hidden; Javascript is required. | (304) 543-8932 | (304) 212-0422 | Andy Travis | Email hidden; Javascript is required. | (304) 951-0909 | (304) 212-0415 | Andy Travis | |
Time | State | Township/City | Pad | Latitude | Longitude | 911 Address | Weather | Well Lease | Well # | Well Field | Personnel/Witness Name | Personnel/Wittness Phone | Company | Position | Hitch Days | Years Oil/Gas | Years w/Comp. | Task | Summary | Spill Amount | On containment | Spill contained | NNE Contacted | DEP Contacted | Spill Line Contacted | Notification Timeline | Spill Cleaned Up | Follow Up Required | Corrective Action | Supervisor Name | Supervisor Email | Supervisor Phone | Supervisor Office Phone | Comp. Man Name | Comp. Man Email | Comp. Man Phone | Comp. Man Office Phone | NNE Name | NNE Email | NNE Phone | NNE Office Phone | NNE Name | NNE Email | NNE Phone | NNE Office Phone | NNE HSE Name | NNE HSE Email | NNE HSE Number | NNE HSE Office Phone | SUBMITTEE |